Log of Jill's 560 SL's life with us.

December 2004–January 2005

Whenever driving by, saw car floating around a used car lot. Giant windshield-posted price didn't look all that bad, assuming I read it correctly. Kept seeing car.

Monday, January 17, 2005

Truly filthy weather, snow and slush piled all over. Rotten for convertible selling. Stopped and looked at car up close. Hmm, interesting. Posted price is in a reasonable range.

Tuesday, January 18, 2005

Jill looked at car. Jill bought car! Technically. (Her name is on it, since it's replacing her 450, which is in her name. She even wrote the check.) Honey, it's not my fault! $11,300, plus the state's cut. I hope to recoup a substantial fraction of this out of the sale of her 450 in the spring. (That, of course, is up to her, both cars are hers. But I don't expect her to want to keep two SL's of her very own.)

Wednesday, January 19, 2005

The car sat at work overnight. Today at lunch I drove it home. In some of the more open areas of road I stomped on it, and it behaved well. Good power, no additional problems noted other than the engine temperature reads a bit low. Does sound like maybe it needs motor mounts, there's more motor noise than in my (same-year) SL. We then all went out for lunch, and Jill dropped me off back at work.

Thursday, January 20, 2005

The battery is/was low, they'd had to jump-start it at the lot once. (I wasn't there.) So I put it on the charger. It's been drinking 5+ A for a couple of hours, and is still thirsty. They didn't know how to jump-start an SL from the hood area, so they'd opened up the battery box and left it that way. I buttoned it back up properly. One thing: the car does have the correct Group 49 battery in it, it looks like a dealer item as the protective flap is attached. While in the area, I found another trunk-mount cell phone antenna. More crap to remove eventually.

I pulled the nasty dash mat off, and peeled loose most of the velcro. The dash is cracked, but not as badly as her 450's had been. I'll clean off the glue later. I want to try filling the crack with Leatherique crack filler, and painting the dash black. It'll have to come out to do this right. Someday.

I had a look at the fuse panel, and found two nasty clip-on connections in there. Either for the stereo or the cell phone, probably the latter. I'll be removing them at some time. No sign of bad fuses, though, will have to look elsewhere for causes of non-functionitis. The driver's door light problem turned out to be the switch. I pulled it out and gave it some good shots of contact cleaner. That restored its function.

The trunk light fixture had no bulb in it. I put one in, but still nothing. The switch plunger was very sticky. I removed the fixture and tried the contact cleaner, but no dice. The plunger might have been a bit deformed, so I disassembled the switch and reamed the plunger's bore out with a drill bit. That fixed it, and now the trunk light works properly.

I got out the Arctic White touch-up paint (for the SDL), and fixed a few rock chips I found. Same year, same color! While I was at it I glued back down a piece of door weatherstrip that was starting to come loose.

Friday, January 21, 2005

The auxiliary fan runs all the time, so I disconnected the temperature sensor for it. I've seen this before, it had happened on my SL once so I'd ordered another sensor. But the problem went away before the part came, so I've still got the extra sensor laying around somewhere. I'll install it later.

To keep the battery charged, and as the car sits outside for the time being, I bought an inexpensive (on sale!) solar panel for the car. I hope this'll keep the battery charged.

Sunday, March 20, 2005

With the completion of the Frankenheap's annual (?) tour of duty, it was time to move on to the next car in the roster: this one. When I went to start it, in spite of the small solar panel I'd installed some time ago the battery was too low. Either something's sucking a lot of juice, or that solar panel wasn't working. I suspect the former, so I'll dive into that. I don't like the stereo that's installed, and there's a big cell phone to yank out too. I put the charger on for 20 minutes so that I could get it started to move it inside.

The car does leak ATF (I think.) There's quite a puddle under it. I shoveled some dirt over it to soak it up. Nice.

Once the car was parked in the garage, I popped the hood and used Super Trim Adhesive spray to re-glue the parts of the hood pad that were coming loose.

I put the battery charger back on, and it took a heavy charge for hours. I left the charger on overnight, it'll shut off automatically when it's done charging.

Monday, March 21, 2005

The heater fan squeaked, so I removed it from the car and lubricated its bearings with ATF. This is pretty easy to do on a 107. One of the two bearings is obviously shot, as there's some play on that side. We'll see how long I can keep this running, as a new blower motor is very expensive. I wonder if it can be disassembled enough to replace just the bearing, or if I can even get a bearing for it at the local bearing supply house?

On the way to work the fan was quiet. Success! (At least for now.)

Tuesday, March 22, 2005

Deciding which of the short list of items needing attention is the most irritating can be difficult, but I thought that the wind leak behind my ear was the worst so I tackled that first. To do this required lifting off the hardtop, which exposed another problem: The release lever for the retention pin didn't work. With enough yanking on the top I got the hook to release and the top lifted off, so I changed plans and tackled that problem first. The cable for the hook was intact and operating, but it didn't have enough range of operation to completely pull the hook back out of the way. Fixing this only required shifting the cable inside the retaining clip that holds it in place. This moved its range of operation to be more usable.

With that fixed, I took a look at the soft top, advertised as being in good shape. It appears to be, but there is a tear in one of the corner windows. It's blue. Next up was to use weatherstrip cement to fix the small tears in the sealing strip for the top stowage compartment. That was easy. Then I was able to actually tackle the wind leak at the three-way joint of the window, top, and body. The weatherstrip had started to tear there, and it had shrunk enough to open up a gap. I glued the tear back shut, and cut some pieces of old EPDM rubber weatherstripping to shim the gap. These attach to the bottom of the hardtop.

With this addressed, the next-most irritating problem was the occasionally-spastic ACC system. It seems to work, but has the symptoms of a rotted foam hose. (I didn't get that far today.) It also sometimes made a screeching relay noise behind the PB array, which can signify that the PB array is in need of a resoldering.

So I pulled the PB array out, and opened it up. No severe solder cracking was visible, but the joints for the relays themselves didn't look good. Using a very hot iron I was able to re-make these connections so that they looked better. I also used a regular iron to touch up all other joints, and I sprayed contact cleaner into the switch array and cycled it a bunch. While reassembling the panel, I checked the lamps and found the one that sources the fiber optics to be out. I replaced that while I was there.

Putting the top back on, I noticed that the sunvisors moved too stiffly, so I loosened their hinge screws slightly to make it possible to (using both hands) get the visors all the way against the ceiling. (Too loose and they'll fall down on bumps, too stiff and you can't push them up all the way due to their double-jointedness. So it's a fiddly little adjustment.)

On the way to work the wind noise was much reduced, and there was no sign of the screeching relay noise. (More time is required to be sure that's been fixed.) But I still think the foam hose is rotted. I'll look at that tomorrow. The center vents also blow heat, as do the defroster vents even when set on EC. A vacuum problem, probably torn actuator diaphragms.

Wednesday, March 23, 2005

Jill drove the car last night to orchestra practice, and received several compliments on it, some of them quite emphatic! That's nice. While she's no car nut I think she enjoys that sort of attention, and it helps her to tolerate, if not necessarily appreciate, my efforts on the car front.

Anyway, she noticed a few of the items I'd already noticed. Nothing serious except she also thinks it handles a bit squirrelly. (She's the first to drive it on the freeway.) I'll have to look into that, it's probably out of alignment or something.

What I noticed after she got back is that the antenna was stuck partially up. So this morning I removed the mast and found it somewhat bent and binding. And gummy. So I did an elaborate cleaning, involving sluicing it out with a succession of acetone, Simple Green, Tide liquid laundry soap, and waterless hand cleaner. A lot of dirt and grease came out in all these steps, but it finally cleaned out. I used a final acetone wash to get out all the water, did some (I hope) corrective bending to get it straighter, lubed it with spray silicone, and re-installed it. That took a lot of time, but now it seems to work right. I think it was the usual tired old story: PO finds the antenna getting sticky (actually due to dirt), starts lubing it inappropriately, finds the problem getting worse, and eventually gives up with the antenna sticking out a lot, whereupon it gets bent in a parking lot—Game Over.

Next up was to examine the foam ACC hose. It's easy to pull the glove box liner to see. And it was rotted! (It's nice when a diagnosis pans out.) I already had the necessary pipe insulation from previous car repairs, so it was an easy matter to cut another length and install it. Then I put the glove box liner back. That should cure its cabin temperature regulation anomalies.

Still with some time left, I unscrewed the cell phone mount from the console tray. It's a big old analog cell phone, and took up the whole tray. My wife requires only two things of a car beyond the basics: that it have a working radio, and that it have a useful cupholder. We have a very useful (though homely) sit-in-the-SL-console weighted cupholder from her 450 SL, but it had no place to sit with the cell phone there. I disconnected the handset from the mount, then I unscrewed the mount from the floor of the tray and found the tray carpet pretty well mashed and gummed up underneath. So I pried out the carpet and gave it a good wash. That nearly eliminated any signs of there ever having been a phone screwed to it. The cupholder sits nicely on a cloth in the tray now, and the cell phone mount is draped behind the seat for now. Actually removing the mount completely will require removing the console itself. This will wait until the dashboard comes out (as it's a necessary precursor) for crack repair and vent pod replacement. That might be awhile!

To finish off the morning, I reinstalled the chrome seat hinge cover piece that I found in the glove box, and pushed back into place one of the plastic hinge trim pieces of the armrest. Tomorrow I think I'll pull the steering wheel and the instrument cluster, to tackle the clock and intermittent wiper problems.

Thursday, March 24, 2005

This morning I emptied the trunk of all of yesterday's shopping booty, and decided to do something about the (non-)spare tire while I was there. What was in the well was a loose tire, and a chromed alloy wheel was in the trunk itself. (Also there was the official toolkit, which I've never seen in any of our other used MB's!) This wheel had chalk circles on its inner surface, corresponding to some very bad pits on the inside. My guess is that the tire developed some slow leaks due to these pits and was retired (!) at that point. (I'm wondering if I can repair these pits using the aluminum welder.) These pits are unusual, I wonder if they're due to flat sealant or something? Anyway, I removed this stuff and put in one of the summer wheel/tires from the 450 SL as a temporary expedient. It's a 14" wheel rather than the 15" that belongs there, but at least it's round and alloy and ought to bolt up OK.

Next up was to address the front lighting situation a bit. I found that one headlight fuse (that also runs the nonexistent fog lights) was blown, so I replaced that. I also found that one turn signal bulb was in backwards, and that the other wasn't fully seated. (These lamp housings are badly damaged, I think due to a curb incident that also took out the fog lights.) With this put right, all the lamps on the car now worked properly, and the lamp-out indicator stayed extinguished. I also adjusted the high beams upwards a bit, as they were lighting the road surface too much last night.

Finally I got to pulling the steering wheel and instrument cluster. This went just fine. I accidentally flashed the clock power lead against ground, and it sparked and blew the fuse so I know the defunct clock was getting power. When I removed the tach/clock pod from the cluster, I could see some burn on the circuit board of the clock. The clock is fairly easy to remove, you just have to remove its hands, all the relevant screws, and the faceplate of the instrument. The faceplate then pivots around the tach needle shaft enough to give you room to remove the clock. Then you apply heat to the ground pin with the soldering iron and the clock pulls out of the pod. Unfortunately, while setting the clockless pod aside I heard a clatter, and looked to see that the tach needle and faceplate had fallen off. No problem, except that some of the tach's shaft was still in the needle! Oh crap, the tachometer shaft broke in half!

Sigh.

Ignoring that for the moment I looked at the clock. There is a resistor in series with the clock's power line that had overheated and burned itself and the circuit board underneath it. I pulled the two 100 µF/16 V electrolytic capacitors, and found them both shorted. This is an unusual failure mode for these, usually they open up, drop in capacitance, and/or develop a lot of series resistance. Because both parts were shorted, clock power through the resistor was shunted directly to ground. This was too much heat to sustain, and it cooked. (Good design would dictate that a larger-wattage resistor be used in case there was such a short. Not enough current to blow the fuse, but too much to dissipate safely. Bad!) Some scrabbling around in the junk box yielded a couple of replacement capacitors that tested out OK on the bridge and the leakage testers. I soldered them back in place. I couldn't read the burned resistor's color code anymore, but I measured it and found that it was still 200 Ω, a reasonable value. So I grabbed a junkbox 220 Ω resistor and put it in place. (Some extra work was required to bypass all the burned traces.)

Applying +12 V power (current-limited to 100 mA for safety) resulted in a small current draw, and the sight of the gears moving in pulses. It worked!

Clock reassembly was uneventful. And now for that $#@*! tachometer.

My spare parts pile included a spare instrument cluster from a 116 gasser of some sort. (Bought because it's the same thing as a 107 cluster, and even has a 107 part number.) Looking at it showed that its tachometer was constructed similarly, but was 10 years older and had a slightly different part number and frequency rating. (I think it was from a 280 6-cylinder car.) Figuring that I really had very little to lose (except my spare $20 cluster), I popped the needle off of this tach (using two spoons as pry bars) and unsoldered the circuit boards from both meter movements. Then I swapped the meter movements and resoldered the boards back in place. Then it was just a matter of reassembling the pods and clusters. While I was there I cherry-picked the best looking meter needles for the car.

While looking at the other cluster, I also checked the resistor in its clock. Turns out it should be a 120 Ω resistor, but the 220 Ω I used seemed to be working and I was running short on time.

Reassembly went fairly well, though it's tedious. With the car back together I replaced the fuse and found that the clock was now working. I started the car and the tachometer seemed to be behaving itself. On the way to work in the car I noticed no tachometer anomalies, so maybe I was able to recover from my mistake. Whew, that could have been expensive!

I checked the SRS lamp bulb, and it was OK. But there's still no power-on indication, perhaps the SRS brain has been unplugged? They may have had an always-on SRS lamp, and disabled it that way. Will bear checking out, it may be that the same thing that was wrong with my SL is wrong here: dead accumulator capacitors in the little box in the wall cavity behind the driver's seat. An easy fix, if it is.

Except for the vent control problem, the ACC system is working fine. It's now set-and-forget, as it should be.

Friday, March 25, 2005

This morning I pulled the driver's underdash panels, to access the intermittent wiper relay and the airbag connectors. (Silly me read the manual first, which said that the airbag connector was under the passenger floorboard. So I pulled that out, only to find nothing like that there. At least I got to vacuum under the carpet.) The wiper relay was broken off in its socket! Looks like somebody must have kicked it, though it's pretty hard to get a toe on it. Anyway, I pulled the piece of PCB with the pins on it out of the socket, and fishing around behind the carpet yielded the body of the relay. I removed the relay cover and super-glued the pin-holding PCB back together, then I unsoldered this board from the main board, which is at 90° from the broken board. With the broken board separated, I was then able to scrape the solder mask from over the trace breaks and bridge the breaks with solder. Finally I soldered the board back to the other one and snapped the pair back into the cover.

Upon installation back into the socket, the wipers then functioned perfectly. Success!

With the under-dash panels all removed, I was able to liberate the little fiberboard side kick panel, which has a vinyl skin glued to it. The glue had failed, and the vinyl was all wadded up and torn. Using spray glue, I was able to glue it back more or less in place, which from a distance makes it look good again.

A similar repair was conducted on the fiber panel that is closest to the firewall. This had been installed improperly at one time, and one end was folded over and half torn loose. Some super glue and a crimped-on metal splint restored it to normal form.

I checked the two red airbag connectors, and with either one unplugged (or restored) the SRS lamp still refused to light. The SRS system may or may not be working, all I know is that the lamp bulb is good but doesn't light. I'm going to have to check out the two boxes in the side wall behind the driver's seat, and probably the main SRS box inside the console. That'll wait until the console comes out sometime.

With nothing left to do in there, I then reinstalled all the under-dash covers.

Monday, March 28, 2005

Jacked up the front of the car via the crossbeam to liberate the front wheels from the ground. No sign of particular wear on tie rods, etc. to cause squirrelly steering, so I'll take it in for an alignment. I know this guy, he's mostly retired and works out of his garage now, but only on cars he likes. Such as SL's!

While I was there I noticed that the brake bleed screws were missing their rubber caps, so I put some on. (The front, I haven't looked in back yet.)

During the day I managed to find (on-line) a manual for the wretched Sony CDX CA-400 CD player that's in there, only to find there's no way to turn off the stinking beeping! The CD player beeps after key-off, to alert you to the necessity (not!) of removing the detachable faceplate. This has sealed its fate, it's coming out! (Someday.)

In the evening I noticed that the headlights still are out of adjustment, so I tweaked on them some. This will be a gradual process, I think.

Tuesday, March 29, 2005

Took the car in for an alignment to address the squirrelly handling. The bad news is that both lower ball joints are completely unsealed, and rusty. Shot, that is. He was able to get it handling a bit better, but strongly advised against driving it much before getting it fixed. He'd be willing to fix it, but he doesn't have the special ball joint press for these cars. Oh joy, more fun for me!

Tuesday, April 12, 2005

Took the car in for new lower ball joints. (I'd researched the ball joint press idea, and found it to cost more than I was willing to spend. The tool price has gone up, from expensive to really expensive!) The car had begun to squeak a lot. (We kept it off the freeway during this time, I just commuted back and forth to work in it since it was licensed and insured, unlike many of our other cars. [To keep costs down, we run them in shifts.])

Wednesday, April 13, 2005

Mechanic called, said it needed an idler arm bushing kit too. While I've done this on an SL already (so I know how), I'm a bit short of time right now. So he's doing that too.

Thursday, April 14, 2005

Picked up the car, the bill was about $475. Handling is much improved, now I need to get it aligned again.

Friday, April 22, 2005

Weather is very good, so the top came off for today. While in the area, I used touch-up paint on the hardtop pecks on the horse collar. Also, there has been a persistent squeak on the passenger side, so I lubed the pivot points of the soft top, and greased the latches of the seatback. We'll see if that helps.

Sunday, April 24, 2005

Yesterday I bought ($4) a center rear seatbelt at the U-Pull, it came out of a '85 500 SEL. It's a bit odd for a 107, but it fit well enough into the back deck area so that our son's car seat can be tethered in place for family outings in the convertible. When not in use, it'll tuck back underneath the deck out of sight.

Monday, April 25, 2005

Yesterday I bought ($6) a new M117 air cleaner housing at the U-Pull. The one in the car appears to have been attacked with an aggressive cleaner (lye?), and has a mottled appearance. While the new air horn is on the wrong side of the housing body, the cover appears to be the same (though it bears a different part number). I just cleaned the new cover and swapped it, for a nicer looking underhood appearance. The body (sides) are still mottled, but that's not as noticeable.

Tuesday, April 26, 2005

The free-standing cupholder from the 450 SL worked great (it's weighted down with an old timing chain), but was a beige color that seriously clashed with the blue interior. Yesterday I bought a 99-cent rattle can of dark blue vinyl paint at the liquidator's, and now the beige is no more. It looks pretty good, though the "Slate Blue" isn't quite dark enough.

Wednesday, April 27, 2005

Got the car aligned (again), for $40. With the new lower ball joints, this time it 'took'. The alignment guy said that the intermittent click I heard on some turns could have been bad subframe mounts, as they were pretty bad. He didn't see anything else wrong. As a kindness he swapped in a better used subframe mount (or bushing?) for the worst offender, and said that would probably cure it. We'll see, so far I've noticed no unusual noises.

The "560 SL" badge on the trunk lid started to peel off the car, so I carefully pulled it off the rest of the way, and when I got home I washed the trunk lid area and the back of the emblem with acetone. Then I used weatherstrip cement to put the badge back on, and a bunch of spring clamps to hold it in place until it dried.

Saturday, June 4, 2005

With the more-or-less completion of the 450 SL's restoration, this car can now get some attention. As it was warm, I got out the AC gauges and had a look. Dead, dead, dead. No pressure at all. A little bit of diagnosis shows a profound leak somewhere at the compressor. I wonder if this is due to its having been converted to R134a? I've heard nothing good about the durability of such conversions. Regardless, this promises to be a fun-fest!

Thursday, June 9, 2005

I installed the keyless entry system I bought for the car. Easy, and works great.

Wednesday, June 15, 2005

I installed the used right-hand fog light I had bought a couple of months ago. Before installation I (re-)painted the shell black, and straightened out the bent mounting ears. While there I solved the mystery of the exploding fuse: the DPO (or whomever) had taped the wires together when they removed the old fog lights (presumably destroyed in a curb-kissing incident). That, at least, was easily rectified! I still need a left-hand fog light, and at least one turn-signal shell, and both turn-signal lenses.

Next I removed the AC compressor. Easy to say, not so easy to do. I had to jack up the front of the car and remove the fan, clutch, and shroud to make room. You also have to (temporarily in this case) remove the hose manifold from the rear of the compressor in order to get the compressor out. The compressor is held in with four long bolts. There is one bolt holding the manifold to the compressor, and a bolt and a stud holding the manifold to the engine. I then disconnected the two hoses at the car side, leaving 1–2 foot pigtails on the compressor end, put the now-free hose manifold back on the compressor, and corked off all four open pipe holes (using rubber stoppers) to prevent moisture entering the system. (It's handy to keep an assortment of stoppers in various sizes around.) The low-side fitting is on this pigtail, so I then submerged the entire compressor in a tub of water and pressurized the assembly with propane through the fitting. The leaks weren't small, they boiled the water! Some examination showed them to be coming from the joints where the manifold adapter bolts to the compressor body, and not the shaft seal as I had feared. Removing this adapter revealed four more O-rings (besides the two on the hose manifold), two of which looked badly chewed. This didn't look like chemical degradation, more like mechanical damage, but I'm told that this is a classic sign of R134a eating R12 rings. I will purchase six new O-rings, perhaps tomorrow. The existing O-rings are all black, and not the newer green or blue ones. Obviously the R134a conversion was a cheap and nasty one.

Next I used gasoline to flush out the R134a conversion's nasty Ester (so saith the tag) oil from the compressor. This is only the first-stage flush, more steps will be required. Also present was green dye, presumably from a leak-hunting session. I don't know how I'll get all the Ester oil out of the system but I intend to: this system is going back to R12 (or compatible), if only for the benign (and highly functional) lubricating oil associated with it. Ester oil doesn't lubricate too well, and breaks down easily.

The first step in removing the compressor was to remove the idler pulley, and I found it to be a bit 'dry'. Not bad yet, but definitely in need of lubrication. I took this opportunity to try an experiment I'd been meaning to conduct. I took my vacuum oil sucker and wrapped a wad of tape around the end of the hose that would wedge in the spout of a plastic funnel. Then I put a rubber stopper in the center hole of the pulley. Next I fired up the vacuum pump and dropped the pulley into the funnel, and pressed down on it to get a good seal. The pulley seated firmly and the vacuum pump started to draw down. Then I just squirted ATF around the bearing, and watched it get sucked into the bearing. A few sessions of this, alternated with removing the pulley and spinning it, resulted in a quiet, smooth bearing. That should extend its life!

Thursday, June 16, 2005

I went to a local AC servicing shop to buy new O-rings, and they said I needed an odd size, and to get them at NAPA where they got theirs. Oh. NAPA next door said they didn't stock any such things, and sent me downtown to their main store (big pain). There they measured them, and found that they only had two in the R134a variety, at about $0.80 each, and it could be weeks to get more. They had a bunch in a slightly larger size, which could (just) be made to fit in place, but they were $4.40 each! No, thanks. I settled for four more of the right size, in black (R12), at $0.77 each. That'll do, as I'm intending to use R12 (or compatible) in it anyway. Annoying that I can't make it R134a compatible in any kind of timely fashion, but c'est la vie.

Friday, June 17, 2005

I put a splash of R12-compatible oil in the compressor and worked it into the mechanism, and re-installed it using the new O-rings. Then I put back the fan, clutch, and shroud. I left the AC piping disconnected, and corked off. I'll vacuum it later, and add a measured amount of oil. I have decided against a full flush, largely because it's so incredibly time-consuming.

Saturday, June 18, 2005

I added about 100 cc of R12-compatible mineral oil to make up the balance of what a 'dry' Nippondenso 10P17 is supposed to take (120 cc), and vacuumed the system for about an hour and a half. While vacuuming, I put a heat gun on the drier to try to drive moisture out of the desiccant. I then charged the system with test refrigerant and it seems to be holding pressure. Vent temperatures were 41 °F, though ambient was only about 70 °F. Further use on hotter days will be the real test.

Wednesday, July 13, 2005

We're preparing for a cross-state road trip in the car, and I decided to put one of our Peltier-effect coolers in the back bucket to hold snacks, etc. Unlike the SDL or the truck (our usual road-trippers), the SL only has one lighter socket; we often use two: one for a cooler and one for a cell phone. While we could use one of those splitter devices, access to the SL's socket is awkward, and cable clutter would end up very annoying in the limited space that's there.

On the other hand, there's a completely unused (in the summertime at least) high-current connector in the back of an SL: the window defroster socket. So what I did was to take a two-conductor connector pair from a boneyard 123's sunroof motor (it's the same connector) and connect the two sets of wires together. This made an extension cord of sorts for this socket, which then in turn plugs straight into the back of a boneyard 115's lighter socket (which also uses the same connector). After cleaning (Dremel wire brush) the inside of the lighter socket and dressing the wires, the result is a nice little foot-long extension cord that hangs out of the side wall of the SL, looks decent, and supplies +12 V power to a standard lighter socket on demand. Into which we plug in the cooler.

It works fine. Of course, we'll have to keep an eye on the defroster switch lamp: since the thing is on a 20-minute timer we'll have to periodically turn it back on during our trip. A small price to pay for less clutter in the car, methinks. If it doesn't work out, we're not out any money, all these parts were free, or next to it. And we can always plug the cooler in up front in a pinch.

I also removed the intermittent passenger door light switch, and drilled out the rivets holding it together. I found that one of the two contacts inside was deformed, probably during manufacture, so I cleaned and reshaped the contacts and put it back together with screws. The interior lamps now work correctly every time. Semi-significant because this also drives the factory car alarm.

Thursday, July 14, 2005

Took a nice leisurely trip to Lake Chelan, top-down and going about 55 MPH on scenic back roads. Just like my SL, such conditions favor good mileage and this one also turned in 21 MPG, with the AC on the whole time! (Which worked well.)

Tuesday, July 19, 2005

Removed the intermittent window switches, and cleaned them out. (The contacts were very dirty, and usually required much cycling to get the windows to come up.) Replaced the rockers (with the worn-off legends) with good used rockers from boneyard 123 rear window switches. The switches now look and work like new, for $4 (the price of the two boneyard window switches).

The pin holding the rear of the shifter surround into the console had been broken off and glued before. The glue failed, so I re-glued the pin back on with Shoe Goo.

Thursday, July 21, 2005

The horn has always sounded weak, so I jacked the car up to have a look. Both horns looked OK, so I removed them and tested them on a battery. The low-tone horn did not work, though sometimes I could get it to go with pounding. Shooting it full of contact cleaner (through the adjustment screw hole) made it worse, and it was totally defunct after that. Nasty-looking (rusty?) fluid came out of it with shaking, I imagine it got filled with water or something at one point and was in pretty bad shape internally.

Interestingly enough the bad horn was a Hella, while the other one was a Bosch. Looks like one of these was a replacement already.

Anyway, what's the point of having parts cars if not to rob? I removed the low-tone horn (Bosch) from the 124 300TD in the woods, and tested it. It worked. So I installed it in place of the bad horn, using the old mounting bracket (which is not straight on a 107, unlike the 124's). Success! The missing low-tone horn is the louder of the two, so its loss was pretty significant.

Saturday, July 23, 2005

Since the old SL got itself washed and waxed, it was looking a lot sharper than this one, so today I washed it. That helped a lot. I also used touch-up paint to take care of the small nicks I found. (Maybe I can wax it tomorrow.)

While drying it I noticed that there was a quarter lodged in the defroster grille, so I tried to lift it out with a forked stick (you can't reach in there with your fingers), and promptly knocked it down into the duct!

Crap. At least I could still see the thing lying on the floor of the duct, it hadn't gone down into the guts (yet).

I then got a section of tecalan vacuum piping (stiff, flexible, and non-scratching), and found that I could just fish it in and touch the quarter with it. I then put a small blob of weatherstrip cement on the end, and guided it back down to touch the quarter near its edge. I then waited for a minute, and then lifted slowly. The quarter came out! I was really sweating that one, but it worked out fine.

Still having a little trouble with the passenger-side window switch, so I removed it and cleaned the contacts again. That seems to have cured it.

Sunday, July 24, 2005

Waxed (Carnauba) the car.

Friday, August 5, 2005

Jill noted last night that the glove box light was sometimes coming on by itself. I checked today, and found that one of the hinge screws was loose, preventing the door from closing fully, so I tightened it. Much better.

Since I was there in the garage, I got out the NOS fog lights I got on eBay recently ($58 for two, a screaming deal!) and had a close look. The lights are new, but the lenses looked somewhat used. No big deal, just dirty/fogged. (One looks like a lamp burned up in it.) Not pitted or anything, and the reflectors and lamp bodies looked good. I took the lenses off and put them in the dishwasher!

...The dishwasher didn't touch the fogging, so I put them in the laundry sink and put in a strong lye solution (drain cleaner) to sit overnight.

Saturday, August 6, 2005

The lye didn't even touch the fogging, so I'll try again with a strong acid instead. Sheesh!

Monday, August 8, 2005

No, acid doesn't touch it. If it is tungsten (or tungsten oxide) from a lamp explosion incident, it isn't supposed to be touched by any acids I want to mess with! (Thank you, Internet. A mix of strong nitric and hydrofluoric [!] acid will eat tungsten. Mmmm, tasty!)

So, I was left with mechanical means. I used some fine wet-and-dry sandpaper, and a small screwdriver to sand/scrape off the worst of it. You can still see it, but only if you look closely. Standing in front of the car it's now invisible. I did scratch the inside of the glass a bit, but it's much less noticeable than the original spiderweb appearance of the fogging.

Then I put the two new lights on the car. They look nice!

While I was under the bumper, I had a look at the cracked air dam. (Probably from the same curb incident I theorize took out all the lights.) The original glue on the back side had cracked and was falling off. Probably epoxy, or something equally brittle, not good for fixing fiberglass anyway. I took some acetone and cleaned out the crack as best I could, then used some good gap-filling cyanoacrylate glue to stick it back together. Then I used Shoe Goo to pot the whole backside of the crack, as this is where any strength of the repair will come from. The cyanoacrylate glue is just to hold it together in place while the other glue sets up, and to fill the crack. With that in hand I used touch-up paint to cover the crack. It doesn't show anymore, unless you're looking for it.

If this doesn't hold up the next try will involve actual fiberglass. I hope I don't need to go there, it's messy, and I'd need to buy more as I'm out of that.

Sunday, August 21, 2005

Jill has been complaining about the sun visors falling down a lot, and the little strips of paper I wedged in there don't help much. So I took out one of the retaining clips and found it cracked (no surprise). I cleaned the plastic with brake cleaner and fired up the plastic welder (hot air blowpipe) to have a whack at it. I was able to get the cracks joined up a bit using the hot air, and then I potted (lightly) the area in Shoe Goo. I glued the tapered washer from the retaining screw into the clip, as the spreading force from this when it's tightened down is one of the things that induces cracking. This went well enough that I then did the other clip. The glue is now drying, but if it worked the body of each clip is not so splayed out, and should grip the visor stub better. Time will tell! The sunvisors are one of the worst design features of the car IMHO. They're fragile, and expensive.

Thursday, September 8, 2005

My wife has been complaining that the turn signals are too dim/quiet, and as a result end up left on more than she's happy with. (This is one area where the older 450 SL is superior: the clacker is louder, and the instrument panel indicator lamps are larger. I also find that the stalk is in a better relative position on the older-style steering wheel, but there's likely little that can be done about that.) The stock clacker is just fine when the top is on the car, but with the enhanced noise floor of top-down driving a louder signal is called for.

While making the lamps brighter is likely not possible, at least without the risk of melting plastic, the clacker is susceptible to modification. I took a look at the ETM's schematic, and decided that it would be very easy to tap the required signal at the hazard flasher switch, which is quite easy to get to on the 107. So, I removed the shifter surround and raided the junkbox for a small 12 V relay. This I glued (Shoe Goo!) to the bottom of the wooden surround panel, right between the hazard switch and one of the window switches. The panel should serve as a sounding board. Then I ran the two relay coil wires to small loops of stripped wire that were lassoed around the 31 and 49a pins of the hazard switch. Voila! A louder turn signal clacker. We'll have to see if it's now loud enough to satisfy my wife. If not, I'm sure I can do better, such as with a larger relay (a standard Bosch automotive relay, probably).

...According to my wife, the enhanced clacker works just right. At first the extra noise disconcerted her, due to its slight time delay and spatial separation, but she says it is adequate to notice when they've been left on, even on the freeway—which was the purpose of the exercise.

Saturday, October 1, 2005

According to me, the enhanced clacker does not work just right. Sigh. I put the lid on the car today, because the weather was bad and I was going on errands alone. (As a family we usually use the SDL.) The clacker causes a small whine to come from the turn signal relay, unless the turn signals are on! This was unnoticeable with the lid off the car, but is far too noticeable with the lid on. Obviously the circuit is too simple in its current form, but I have hopes that a cure won't be too difficult. (The clacker's coil resistance is too low, and the turn signal relay is sensing its presence, and reacting to it.)

Looking at the car's schematic again, Plan B is to place the clacker relay between the R and L terminals of the hazard switch, using the unlit side as the relay's virtual ground. (The operating current of the relay shouldn't be enough to cause any wrong-side lamps to light.) This operation is simple, and only requires moving the wire lassos on the hazard switch.

If that doesn't work, Plan C is to use diodes to combine the R and L terminals (in conjunction with the real ground at pin 31). Plan D reverts to Plan A's wiring, but uses a transistor or two to amplify the signal so that the load on the turn signal relay is reduced. (Switched power is also available at the hazard switch.) If that doesn't work, Plan E involves modifying the turn signal 'relay' itself, probably by putting the clacker in parallel with the real internal relay. (Plan F is just to rip all the crap out and call it a bad idea.)

Plenty of plans, one of them ought to work!

Sunday, October 2, 2005

Plan B worked, according to, ahem, plan. I moved the lasso wires to the L and R terminals of the hazard switch, and the clacker still clacks, the signals all work right, and the whine is gone. Using a virtual ground this way, the extra clacker doesn't clack when the hazard lights are on, but that is of no consequence. It's possibly even preferable.

Monday, December 12, 2005

The used turn signal I won on eBay came in today, but an edge was chipped off the lens. So I glued it back.

Tuesday, December 13, 2005

This morning I installed the turn signal. The other side still needs a lens, and I suppose I'll need to buy that new.

Monday, January 16, 2006

Put the car on the battery charger for awhile, then hooked up a battery tender. We're not driving it, so it really needs this bit of TLC.

Tuesday, August 22, 2006

Won an eBay auction for two used turn signal lenses, $16.01. Much better than the pairs of lenses that have been showing up for $46/pair (plus shipping) for the last six months.

Wednesday, September 6, 2006

The two eBay RF turn signal lenses showed up today, they look good. (Better, in fact, than the LF replacement lens that's now on there, but tucked under the bumper as they are it's not that easy to tell. In fact, the major objection to the POS substitutes that were there when we got the car is that they're not weathertight, not that they're particularly ugly.)

I put one on the car in place of the ugly aftermarket plastic sheet. The POS was held on with the original screws, so I transferred them to the eBay lens that didn't come with screws, and put the other one on the shelf as a spare. Looking good!

Tuesday, May 15, 2007

With the sale of Jill's 450 SL it was time to dig this car out of storage. It was filthy, but it had been on a battery tender so it started right up. I drove it into the lawn and washed it. What a transformation! I dried it off then put it back in the garage to lift off the top. (Had to do some cleaning under its rim.) Drove it to work, and at lunch got it emissions tested and licensed. Nice car. Stupid sunvisor keeps dropping down on bumps, though, and the keyless fob seems to have forgotten its purpose in life.

Wednesday, May 16, 2007

I put on the new license plates (stupid State, there's absolutely nothing wrong with the old ones, I think they just do it to get more money periodically), then cleaned up the trunk, sorting out what had come from the 450 SL (which I had thrown indiscriminately into it). I vacuumed it out and put in a set of (miscolored) floor mats, I'll get a better-matched set later. The car has a ratty steel spare, with associated lug nuts, so I tried (again) to get its alloy wheel fixed up. We got the tire dismounted (PITA!), but the inner tube I procured for it needs a buffer pad as the inside of the alloy is a bit rough where last year I tried, unsuccessfully, to weld up the pinholes. Later, I guess.

I installed the new hardtop front mount washers. (That's always surprisingly difficult.) I also put a piece of plastic sheet into the loose sunvisor socket, that should tighten it up a bit. When I got out the spare fobs and the instructions for reprogramming the keyless system it started working again. Weird. The car's all ready for Jill to drive.

... Out at lunch I was buying a battery for the 190D at Les Schwab and picked up a used (dead) inner tube. That should supply some rubber for a protective band around the alloy wheel's inner surface.

Thursday, May 17, 2007

Got the spare tire the rest of the way dismounted. (PITA!) Cleaned out the inside of the tire, and inflated the dead inner tube in order to plan the cuts. Cut out the inside ring of the inner tube. It was too large (of course) to stretch over the hub of the wheel. It was also too wide so I first cut a strip off the side. Then I took out about a 4" section containing the valve stem. This resulted in about a 2" overlap of the remaining strip when wrapped snugly around the hub. I then washed off the overlapping ends with acetone and smeared on weatherstrip cement. (The good stuff.) When that tack-dried I carefully pressed the glued flaps together. After only a short period for that to set up I rolled the resultant band onto the wheel around the hub.

Next I found I had to cut out a hole in the band for the valve stem. I also found that my new inner tube had a shank much too large to fit through the wheel's hole, so, as the wheel was essentially ruined anyway, I drilled out the hole with a 9/16" bit so that the shank would protrude a usable distance once inserted. The hole's still not really large enough, but that's about as big a hole as I can drill there easily.

Then I remounted the tire. (PITA!) I used Simple Green as a spray-on mounting lubricant, and put on the one side. Then I tucked the inner tube into the carcass, pushing it well out of the way of the rim and making sure the valve stem was in the wheel's hole. Then I put on the other side. (PITA! Have I said that lately?) I found that my air chuck wouldn't reach the poorly-fit valve stem, but that another one I had for doing truck tires would. I inflated the tire until the beads popped into place, then removed the valve core and deflated the tire fully. Interestingly, once the inner tube had deflated the tire started making air noises. I think there was air trapped between the inner tube and the tire that was then able to get out. Finally, I inflated the tire to spec. I put it aside where I plan to monitor its pressure for a few days. If it holds air I'll swap it into the car.

Monday, May 21, 2007

I removed the loose driver's seat, and was again reminded that you do not unhook the spring-loaded elevator mechanism. The seat slides forwards (or is it backwards?) off of its studs. Getting that big spring put back into place was a giant pain. One of the two mounts for the elevator's cross shaft is buggered up, and has some doesn't-fit-right US thread bolt wedged into it. Unfortunately a more proper bolt from the junk box wouldn't 'bite' anymore, so I had to leave the mess in place. To take the sting out of this extra chore I found 39 cents under the seat. Woo-hoo!

Anyway, with the seat out I found that there was one (only) of its eight glides missing. I got out one of the new ones (I'd bought a dozen!) and put it in place, cleaned out the tracks and re-greased everything with my old can of Lubriplate. At that point the track was still a bit loose, unlike the other one. I pulled the other one back off and found that half of its glides, the upper ones, had rubber spacer strips inside them, whereas the loose track had none. I cut some strips of inner tube rubber to tuck into the glides, and after that they fit snugly in the track.

With the seat out I also noticed that the metal spine through the leather that the hog rings holding the back of the bottom in place tie to had slipped sideways far enough to release one set of hog rings to pull directly on the leather. Fortunately the leather had not yet torn and I was able to get the spine slipped back into place. I then reinstalled the seat. This, apparently typical for 560 SL's, is not all that easy. But I persevered and got it back into place without noticable incident. It feels a lot nicer than it did, and slides easily. No more rocking.

Then, because it's a rainy day, I put on the hardtop for my wife.

...We met for lunch and I noticed that one of the front tires had tread separation all around the outside! We knew it was time for tires, but not that it needed them that badly. She stopped off at Les Schwab later and put on a set of unidirectional Toyo Turezas, 80 kmi warrantee. About $570. Three of the four tires were crap, but one didn't look too bad. I had her keep that one, we may find a use for it on some car or another. Probably for a spare.

Tuesday, May 22, 2007

Made the extension plug for the embedded garage door opener. This turned out to be surprisingly difficult, mostly because I don't have enough hands. I took a cut-off pigtail connector for a defroster switch and some random bit of a MB relay block (126?) that I found at the junkyard that had male connector pins, and soldered four male and female pins together end to end. (Coming up with male pins is relatively hard, most of these cars' connectors are female, and most of the male pins are embedded in assemblies that don't come apart.) The male pins just fit through the socket's snap-on retainer, and protrude nicely. I then soldered two wires to the 31 (ground) and A (Off) pins. I then built another 9 V regulated battery replacement using a 9 V Zener, a 47 Ω resistor, and the top piece of a dead 9 V battery. (I had left the original in the 450 SL for the next owner, he seemed interested in using it.) I wired this up and put it in the battery compartment of the garage door opener. I also moved the shorting wire to the correct switch on the opener for this car's location. (It's a triple opener.)

So, what I ended up with is a plug for the defroster switch that has pins sticking out the back onto which I can plug the car's connector, no surgery to the car's wiring harness required. (Unlike on the 450 SL's prototype.) The opener is then tucked into some tidy under-dash place. Unfortunately I ran out of time to install it, but I did test it out. Worked fine.

...At lunch today we went to the park, and as it was warm when we were leaving I tried the AC. It works! Apparently it doesn't have a bad leak anymore.

Wednesday, May 23, 2007

I installed the embedded garage door opener. This turned out to be harder than I thought (big surprise!) because I had forgotten how tight the connectors fit through the holes in the dash. There wasn't room for the extension plug to fit through with its wires coming out the side. I had to bore a hole in the car's connector shell so that the two wires from the extension plug could go through it rather than around it. And, of course, with all the messing around one of my two wires broke off... So I ended up having to drag the soldering iron into the car anyway, though avoiding this had been the whole point of making the extension plug in the first place! To avoid having my mated pins fall apart during the repair I clamped it in a vise grip, but with a layer of thin cardboard for thermal insulation so that it could be heated to soldering temperature. It worked. I should have done it that way when making them in the first place.

There is an access hatch in the rear of the glove box, I put the opener behind that so that it might be possible one day to fish it back out without removing the glove box liner. Perhaps we'll see. Or not.

Anyway, once installed it worked perfectly and I took the roof off the car in celebration. (It's looking like a nice day today.) I even found 25 more cents under the floor mat! I removed the loose garage door opener so that my wife will have to test it. I mean, 'retrain'.

Saturday, May 26, 2007

I've been musing on the idea of an appropriate Road Trip Relay for this car. Two years ago we took it on a nice road trip and I used the rear window defogger plug to power the cooler. However, the automatic power-off cycle of the timer relay was a minor problem. (In the sunlight you couldn't really see the lights turn off because the relay had timed out, and in an open car you couldn't hear the cooler's fan stop.) I'm hoping we will take other such trips in the future, and I would like to improve this situation for next time. Since I have a schematic for the 107 820 00 10 defogger timer relay, and some experience modifying it, I've been musing on potential modifications for this car. While the delayed shutoff of the 190D's additional modified relay is attractive it would require some rewiring of the car. Nearly as attractive would be a modification of the existing relay to disable the timer. I have worked up a circuit that would allow you to hold the OFF side of the switch down for a few seconds, which would trip the relay ON yet prevent it from timing out in this mode. You would turn it off, normally, by actuating OFF again or by turning off the car. Turned ON and OFF in the customary manner it would behave as an unmodified timer. Given my apparent inability to design transistor circuits that don't have nasty side-effects I think I need to prototype this before committing to it further. The proposed modifications should fit entirely within the case of the relay. Three transistors (one PNP), four diodes (one a Zener), two capacitors, and five resistors: nearly as much circuitry as the timer relay itself! If I were set up to burn PIC microcontrollers I'd be tempted to bypass all the logic and put it all into an 8-pinner. Wouldn't be much of a program. But that's a lot of infrastructure to deploy just for this application. [See September 18, 2009 for the next installment.]

Tuesday, May 29, 2007

The tubed spare tire is holding air well, so I put it in the car in place of the nasty steel spare (with lug bolts) that was there. Much better!

...At lunch I bought some gray floormats at Costco, to replace the tan (taupe?) ones that were from the 450 SL.

Wednesday, May 30, 2007

I installed the gray floormats from Costco. They're a better color match to blue than the taupe alternative, though I wish they carried a few more colors. I put the little ones in the rear too, as my boy walks through there when we're all in the car.

Sunday, June 3, 2007

While driving us all to a party my wife slapped at the sunvisor and managed to stab herself on some sharp nasty little spring clip somebody had installed to hold the hands-free microphone for the (defunct) car phone in place. That's got to go!

Tuesday, June 5, 2007

I pulled the sunvisor and associated trim off so that I could pull the microphone out of there. I peeled it down the A pillar and just stuffed it under the dash, I'll do more someday when I remove the rest of the car phone. Since it was raining I also put the top on for her. I gave her that sharp spring clip, she didn't seem to appreciate getting it too much! (She did appreciate its removal from the car.)

Wednesday, June 6, 2007

At lunch with the family I noticed a bit of a gas smell around the car. No drips, but I will have to look into that.

Friday, June 8, 2007

I prepped the car for Jill's cross-state road trip to see our niece's Christening. I put the cooler in the bucket and hooked it to the defroster plug. I washed the car, then took off the air cleaner to look for gas leaks. Found some! Two of the fittings on the fuel distributor looked damp, and the body of the electrical dingus on the side was weeping. I removed all these items and cleaned up the seats. That cured the distributor leaks, but the dingus was still leaking gasoline from its weep holes. I went to my convertible in storage and stole its electrical part, and put it on instead. (It must be love!) Other than a fuel fountain or two during installation it looks good. (I put the bad part on my car, to plug the holes at any rate. Also I had to clean the mouse nests off of the engine, sigh. I've got lots to do down there now.)

EHA

Unfortunately I believe this leaker is the E.H.A. valve, and is a $300 item on Rusty's site. Yikes!

She also reported that her window switch had stopped working, so I tore that open and cleaned it. It works again.

...Later at lunch with me, on her way out of town, my wife reported that it was running rough. I took a quick test drive, and it indeed wasn't running too smoothly at idle. (Though the gas leaks were cured.) It smoothed out as it warmed up, so I'm guessing that there may have been a bit of dirt that got into the system when it was opened up, or that the replacement EHA requires a different adjustment setting on the fuel distributor. We'll see how it's doing when she gets back on Monday. A couple of nice long cross-state freeway drives ought to blow out the cobwebs, if anything will.

I did some more surfing, and it seems that Bosch used this particular EHA on most gasoline Mercedes in the 80's-early 90's, though apparently on nothing else. Used supplies will be relatively limited if I can't also shop Audi/VW/BMW wrecks of the era. Some parts sites seem to imply that the 190E uses a different EHA, so they could be out. (This is not particularly clear in my on-line research.) At home I hit my copy of the US EPC for this SL, and came up with a part number and a where-used (application index):

This shows the 190E uses the same part, so I have contradictory stories, unless there are other 190E's. The service manual I have indicates that some 190E 2.3's before '87 use 102.961 engines, and some use 102.985, great! The 2.3-16 is also off my list, if I can believe this chart.

A 000 070 39 62 Governor
102.985190E 2.3  116.965420SEL
103.940300E 2.6  117.964500SL
.942190E 2.6   .965500SE(L)(C)
.981300SE(L)   .967560SL
.983300(T)E    .968560SE(L)(C)
.985300(T)E   119.960500SL
104.980300CE
.981300SL

That's not too short a list of wrecked cars to shop from, though some of them are a bit new to stumble across in the low places I frequent. The 190E's are likely to be the most fruitful source.

It's just that I balk at spending $300 for a new one. It's so small!

Friday, June 15, 2007

I called a craigslist ad. where a guy is parting out a 190E. When we finally got done playing phone tag it turns out he wanted too much for it, the engine was a runner. He knew what an E.H.A. valve was, anyway, and what they cost new. We'll keep looking.

Saturday, July 21, 2007

My wife reported that there has recently begun a horrid scraping from the RR wheel, and today I got a chance to look at it. Yep, one of the brake pads (rock-hard semi-metallic by the looks of it) was worn to the metal. (The other was decent enough still.) I replaced it with a used pad I had kept from the Chicken Wagon for just such an eventuality. That should stave off its eventually-required brake job for awhile. (It's a really quick job to switch pads on an MB, if that's all that needs doing.)

The car desperately needs a new muffler, the bad one on the car is peeling apart and is extremely rattly. If it rattles while removing a wheel you know it's bad!

Jill called from the road and said the sound was gone, and was quite happy about it. The sunvisors are still falling down, however, and she is happy about that, not. She says that she has again received a number of compliments from her orchestra buddies on her nice car, I think she is pleased about that. (As am I.)

Tuesday, September 4, 2007

Daniel's first day of school. (Kindergarten.) My wife came by work to take me out to lunch. Just like a date! Anyway, the antenna was partially up and I thought I'd grab it and work it up and down a bit, cleaning off the dirt with my hands. (I do this from time to time.) The antenna came apart! One of the segments popped out, there's a coppery split bushing that worked its way past the crimped over top of a segment. I couldn't get it back in by hand, I told her not to extend the antenna all the way until I could deal with it. Crap. Oddly enough, my wife didn't seem all that pleased with how it worked out.

Wednesday, September 5, 2007

I pulled the antenna mast out and played with it for awhile. I got it cleaned out some, but I was unable to get it back together with all four sections working. (I think they're crimped together during final assembly, so they're not really repairable.) It's hammered together now such that the one sick section is more-or-less permanently stuck down. It's only three sections now, it could really use a new mast!

Monday, September 10, 2007

Last night the lamp-out warning light was again on, but this time the bumpy road to the house didn't turn it off. (Jill says it's on most of the time.) So I walked around the car and found that the left front side marker lamp was out, and came back on when I thumped it with my hand. Just have to love an intermittent electrical problem! So this morning I pulled the headlamp assembly. The USDOT lamp assembly is definitely a second-class citizen, you need a screwdriver to remove 6 screws in order to get the lamp assembly out, and a wrench to remove three 8mm nuts in order to get the side marker cover off to expose the bulb. How GM! (The bulb was bad, so I replaced it. The difficulty of getting to this bulb meant I used a brand new bulb, not a used one.) What a contrast to the ease, for example of bulb replacement in a 123, 126, or 201 body. Or for that matter, the trunk lights in the 107.

Since I was in the area I tackled the surface rust that was beginning on the crossbrace in front of the fan, and on the vertical wall behind the auxiliary fan dropping resistor. I brushed off the rust, chipped off any loose paint adjacent to it, and spray-painted it. First with primer, then color coat. (Rattle cans, of course.) This has been the only sign of rust on this car, I definitely don't want to let it gain a foothold.

Also, last night I noticed that the LR brake was scraping, so I jacked it up and checked the pads, one was down to the metal on the edge. I replaced it with a good used pad I had, the other one is good for some few thousand miles more. Next time I need to just replace the full set. It's sure easy if pads are all you are doing, jacking up the car and pulling the wheel is the most time-consuming part.

Oil. I finally checked and I've never changed the oil on this car, and we've driven it in excess of 10,000 miles! Oops. I sucked the oil out and put in new. I didn't have time to do the filter too, I'll get that next time. (I usually do the filter every other time anyway.)

Tuesday, September 11, 2007

At our first PTA meeting (?) I noticed that Jill's tire was very low. I had her drive by Les Schwab and they found a nail in it. That was certainly easier to deal with than me having to do anything.

Friday, September 14, 2007

Jill handed me a package of new sunvisor clips. Those remanufactured ones, $50 for the set of four pieces. When we were driving this car this evening her visor fell down several times. She'll allow me until tomorrow to install them!

We'd gone to see Seussical, and Jill commented that she thought the headlights were cutting out at times. I didn't notice anything, but we've seen this before with the SDL. (It was the combination switch going bad and cutting out the low beams on right turns.)

Saturday, September 15, 2007

I installed the new sunvisor clips. Though in sorry condition the old ones went to the 380 SL, which needs one set. (I should be able to paint them black to match.) I couldn't get the old male pieces off and there was nothing wrong with them anyway, so I only installed the new sockets. The other parts can stay in reserve.

Monday, September 17, 2007

Weather's turning colder, I put the lid back on her car.

Wednesday, September 26, 2007

Last night Jill informed me that the car's ACC seems to be heating too much, and that she turns on the AC to tame it. This time of year? Something's wrong. I pulled the monovalve insert and found dried coolant residue in the spring washer, and its solenoid plunger was waterlogged. The seal diaphragm, however, isn't torn that I can see. I wonder what's up with that? I cleaned it out and put it back. (For reference, the assembly order of items into the body is plunger, small washer, spring washer, large washer, collar, and coil.)

Y'know, I'd always thought that a waterlogged monovalve plunger was a sign of failure, but having taken it apart (and another one from the spares pile) it seems more to me like it's supposed to be full of water. There's a weep hole from behind the screen into the plunger area, through the plane of the diaphragm. If the intent is that the plunger fill with (screened) water resulting in water on both sides of the diaphragm, the passage of water through this hole as the plunger moves back and forth could serve to damp the physical motion of the plunger. It may be that the slow-scale PWM signal from the ACC system actually results in a fairly steady physical position of the valve rather than an on-off modulation of water flow. This would actually make some sense in that it would dramatically cut down on diaphragm wear, but then I have no explanation for why a torn diaphragm results in loss of control of the valve. It ought only result in a leak. I guess we'll see if the cleanout has done anything helpful.

Thursday, September 27, 2007

Jill reports that she has noticed no heater anomalies since the laying on of hands.

Wednesday, October 10, 2007

Replenished the brake fluid. Where's it going? No obvious sign of leaks. Could it be sucking it into the intake manifold?

Friday, October 26, 2007

The car's new muffler was delivered today. $265, when bought with another one for my 560 SL. Eberspacher, the good one. Heavy.

Sunday, October 28, 2007

I installed the new muffler. Just bolts on? Right! First, of course, the leprous old muffler had to be removed. (It also looked like somebody had backed it into something like a high curb: besides the big chunks flaking off the outside it was accordioned a bit in the middle—it was long past time to replace it. It was the original muffler according to the 1286 date code embossed into it, and made by Gillett.) The existing bolts were frozen, and even after I got them off (twisting one in half, though I did get the nut off to be reused) the retaining collars were frozen. Eventually I got those loose, and that's when I found out I hadn't ordered the seal bits that go into the pipe joints. One (for the flared mating ends) was ratty but reusable, but the other (for the slip joint) was ruined. I had to fabricate something out of two rings of metal cut off the old muffler's pipe. I slit them and spread them out so that they would fit concentrically and snugly over the new pipe, inside the formed collar that's on the muffler end, then I welded on the edges to fill the gaps. (They were left split.) I then put it all back together, using anti-seize on the bolts. The junk box supplied another bolt to replace the ruined one. It took 2.5 hours or so to do the job. The center resonator's rubber support rings were missing, so I used some of the chain-filled ones from the junk box. (Whenever I see them at the junkyard I grab them.) The resonator, etc., still looked intact.

A big PITA, but it works nicely now. Quiet. Had I bought new seals and bolts it would have gone a lot smoother. Incidentally, my wife still has reported no further heating anomalies, so cleaning out the monovalve last month seems to have done the trick.

Tuesday, October 30, 2007

At the U-Pull for some other stuff, I found another set of heated front seats in a 126. I got them, the mating plugs, and the switch sockets for about $20. (And the cables between them, only the one cut [each] at the three-wire point for power, ground, and illumination.) These are the relay-less early version. The switches were long gone, as was the back seat. One of the butt pads is open-circuit, the other three pads all measured about 5 Ω.

Saturday, November 3, 2007

The squealing from the car has been getting intolerable. The rear brakes are making noise, too! Time to do something about it. I replaced the motley collection of used rear pads with good new ones from Rusty. It gets easier each time. I ground the small lips off of the brake discs, the easy way there is to let the car spin them while you 'kiss' them with the running grinder. I greased the backs and edges of the new pads for squeal-proofing.

I also topped off the brake fluid and engine oil. It seems to be using a bit of both of these.

I had a setback on my heated seats plan. I removed the seat cover from one of my heated 126 seats, only to find that the heating elements are sewn into the covers, they're not separate pads under the covers. Oops! Now I've got two sets of front 126 seats, and one rear seat, that aren't going to be of much use.

...I shouldn't work tired. After lunch and a nap I had another look, and the pads are merely long fingers (like a coarse comb) tucked snugly into the sewn channels. Getting them out will be hard, and into another seat harder yet, but shouldn't be impossible. I'm going to do my experimentation on the dead pad. Who knows, I may even be able to repair it.

Thursday, December 6, 2007

We were going to take this car to the company Christmas party (at the fanciest hotel in town, the Davenport), but Jill couldn't get it started. The dash lights were acting weird, the alarm went off on her, and it wouldn't even crank. Battery? I had no time to look at it.

Friday, December 7, 2007

I put the battery on the charger, and it was seriously low. I wonder what the excessive draw could be, the nasty Sony stereo? We're not driving this car anymore this season, apparently I need to rig it with a battery tender.

Saturday, January 5, 2008

The roads have cleared, so I sent my wife off in this car for a change. She can get it washed, and maybe fill it up. The car is filthy, and appears to have possibly-salty road slime on it from before, I want it off! The battery tender is doing its job, the car started instantly.

The brake fluid was again low, and I had to refill the reservoir. Where is it all going? There were no spots on the floor.

Monday, January 7, 2008

The replacement antenna mast came today. Jill managed to get to the box on the porch before the dog did.

Tuesday, January 8, 2008

I installed the antenna. It took a few tries to get the leader started, naturally. Around the shaft it's a little bit looser than the original, I hope that's meaningless. (It's not Hirschmann.)

Saturday, April 12, 2008

Magnificent weather today, finally, it hit 65 °F, blue skies and all. Got out the car and took the lid off so Jill could take it to a concert in style. I did need to add quite a bit of brake fluid.

Saturday, April 26, 2008

Finally another beautiful day, unlike all the intervening days since last time. I prepped the car to go downtown for dinner, topless.

...Wretched POS! The battery was stone cold dead again. There's something wrong with the car, if not being driven for two weeks can (but doesn't always) kill the battery. I had to take the other convertible, which had not been prepped for the trip, so we were late. I put the battery tender on the car to bring it back up, the charger was busy doing de-rusting duty on the boat trailer's leaf springs.

Sunday, April 27, 2008

The boat trailer springs had finished de-rusting, freeing up the battery charger. I put it on and the car resumed drinking heavily. Obviously the little tender wasn't up to the job; I didn't really expect it to be.

Monday, April 28, 2008

I put the charger on again this morning (I should have done it last night) and it resumed pulling a pretty heavy charge. Poor thing!

...After I got home I put the charger back on, Jill had taken the car out. Still drawing heavily!

Tuesday, April 29, 2008

I checked, and the charger is down to about 1 A or so. Seems to finally be about done. I'll leave it on a while yet to top off. I also need to get out the ammeter and see if I can find a parasitic draw, there is definitely something wrong, though perhaps it's intermittent.

Thursday, May 15, 2008

The car hasn't been driven in a few days, so I put the battery charger on. It drew heavily, and only settled down to about 5 A after an hour. There's something definitely wrong, I wonder if the alternator is charging? I need to check into this.

Monday, July 14, 2008

Jill called me at work from the parking log of Wal Mart. (Not the close one, however.) Said there was a big green puddle under the car. So I headed over there. There was a big green puddle under the car, but I couldn't really see why. Nothing obvious, but the reservoir was pretty much empty. I sent her in for a gallon of water and I poured it in. No leaks, I sent her in to refill the jug just in case. We caravanned home, there were no problems. Just a minor overheating episode on a hot day with her crawling around a parking lot looking for a good spot with the AC on? Let's hope so!

Wednesday, August 13, 2008

I finally got a chance to tackle the battery discharge problem. (I've been putting the car on charge most nights for months now.) I suspect one of the two alarms, or the stereo is at fault. (Though it could be almost anything, including the clock, radio antenna, or dome light system.) I pulled apart the main power supply terminal under the hood and determined that there was no parasitic load except through the main feed wires to the fuse box. (Thus clearing the alternator itself [of bad internal diodes], and the starter.) When I disconnected the keyless entry/alarm system and powered up the car it draws some 200 mA once things settle down. That's fairly hefty, over time. When I dug up the fob so I could reconnect the keyless entry/alarm and shut it up I found that it only seems to draw 10–20 mA itself: not so bad. I removed the trunk light bulb, no change. Removing the faceplate of the stereo did nothing to change the draw. I removed the floor panel, but the factory alarm isn't under there so I couldn't disconnect it. I mis-remembered, it's behind the glove box according to the ETM. (The lamp-out warning module is what's under the floor panel.) I ran out of time to continue chasing this morning, however.

Jill also reports that the headlights spontaneously go out sometimes. That's not good, and it keeps her from wanting to drive the car. Combination switch? I've seen that before, though usually only when applying a turn signal.

Thursday, August 14, 2008

It's not the stereo (removed), or the antenna (unplugged). But it's on Fuse 12. If the schematic can be believed that indicates the antenna, trunk light, alarm system, warning module, courtesy lamps, diagnostic socket, hazard signals, or clock. I disconnected the alarm, that's not it. I pulled the dome light timer relay, that's not it either. I checked the visor lights, it doesn't seem to be them. (Current draw when either was opened was the same, 950 mA, and together it was about 1600 mA. That indicates that neither switch was leaking.) I pulled the door switches, no change. It's not the warning module. (Getting to that was fun.) It's not the hazard switch. All that's left is the clock, which is difficult to get to. So I pulled the airbag, steering wheel, and instrument cluster. It's not the clock! WTF? Supposedly I've gone through everything on Fuse 12, yet I've found no culprits. The car still draws 200–350 mA through the fuse. Damn, either somebody added something (cell phone?) or the schematic's wrong, or there's a pinched wire. The next step is to pull the fuse box itself and check the individual wires feeding off of it. That's a drag.

So I pulled the fuse block. There are two ring terminals screwed to #12: one a clump of small reds with a red/yellow in it, and another clump of small reds with a red/white in it. The culprit is in the red/white clump, though I ran out of time to chase it further than that. The red/white wire itself goes to the diagnostic socket, and nothing's plugged into it. The car now looks a right mess, and it's probably going to get worse before I'm done.

Friday, August 15, 2008

More leak chasing. The schematic shows eight wires on Fuse 12, and there are two ring terminals of four wires each, which bodes well for the schematic being correct. I put a test light in series with the fuse power supply so that slips wouldn't cause big problems, and the offensive current was still about 150 mA. I then used the low-current (60 A) AC/DC amp clamp (a one-time Christmas gift from my brother the mechanic, perfect for digging around in a car's wiring harness as it has much smaller jaws than my 400 A Fluke or the 2000 A OTC that I just bought) and clamped it in turn around each wire in the offending clump at Fuse 12. One of the solid red wires leads to the culprit, which means it's not the clock or diagnostic socket wire. I then grounded the offending ring terminal to reverse the test. I went around the car with a small 12 V battery in series with the test light. I'd ground the battery and then probe for power wires with the test light. When the light lit up I'd look at the meter (perched on the dash) to see if the current was going through the offending wire. No joy at the back of the car, nor at the courtesy lights, hazard switch, radio, or dome light timer. (All customers of Fuse 12.) But when I popped out one of the two dome lights I found my circuit! At least it's a short (!) one, though I was out of time to chase it further.

Saturday, August 16, 2008

Victory! I tackled the other dome light, only to find that it was glued in place because one of the plastic ears was broken off. It wasn't fun getting it loose without tearing up the molding, the whippy thin almost-sharp antique carbon-steel butter knife (one of my favorite tools) worked well. The nylon insulation wrapper on the hot lead was brittle and half missing, and I think it was pinching through the foam insulation on the molding and partially contacting ground, as there was a pit chewed into the foam down to the metal backing. That could make an intermittent, and variable, short circuit. It explains a lot, and the electrical leak was gone once I took this apart. (A good solid short would just have blown the fuse, of course.) I put some Shoe Goo on the thin place on the molding's foam and scraped up a replacement light fixture from the junk box. I used heat shrink tubing and electrical tape to bolster the insulation at the terminals that hook to the light fixtures. That should take care of the problem, and once the glue's dry I'll start putting it back together.

It seems like I had this exact trouble spot flare up before on one of the other SL's, but I just can't remember which one nor can I find any record of it. (That bugs me.)

Sunday, August 17, 2008

I put back the molding and the dome lights. That went easily enough, except that the 'good' used light fixture had bent with heat enough that it would no longer snap back into the hole. I used a propane torch to heat it gently until the styrene got soft then I bent it back into shape. It got a little bubbled looking on the inside, but it's really hard to notice and it does fit back into place. When I checked the wiring for current leaks there were none. Cured!

Then I started putting the fuse box back together. Since I was there I took the opportunity to restore the separate (from low beams) function of the fog lights. (I do this on every car I can as you can actually see better without the main headlights under extreme fog conditions.) That involved moving the gray/yellow/green wire from Fuse 19 back to Fuse 15. I also had to scrape up another fuse box screw from the junk box, relabel the fuse panel's card, and swap an 8 A fuse for the original 16 A that was in Fuse 19. That took a bit of time, especially the scavenger hunt. Unfortunately I was again out of time to do more.

...After church I pulled the combination switch out, and for the first time tried to open one up. (I've replaced a few now, and they're expensive enough that I've wanted to dive into them to see if they can be cleaned up but hitherto I haven't really had the time. Also, it's a critical enough component that I didn't want to mess around if there was any risk of malfunction, but as I learn more about these things I realize that there's actually little risk of that if one is careful and if one is always prepared to buy another one if things do go wrong.) If you're careful you can release the plastic snap clips and it swings open, exposing the contacts. Which in my case were quite dirty. I think this can be cleaned up to good effect, but it's too hot out to enjoy working on the car right now, so I won't.

Monday, August 18, 2008

Per request, I photographed the combination switch so as to highlight the way it opens. On the upper (as shown) sides of the plastic body are two plastic bails that have to be bent away from the contact-carrying plastic 'plug' more or less simultaneously. If you do this right and the bails don't break, the plug swings up and out on its wires, exposing the guts for cleaning. Note the spring-loaded plastic turn signal release flipper at the bottom of the body, and the sliding turn signal contact at the top. The obvious dirtiness of the contacts is not apparent in the photograph. There is a little spring hooked between two pegs buried in amongst the terminal lugs, don't lose that and make sure you hook it back up. (It's what puts spring tension on the headlight switch contacts, and the switch won't work right without it.) You don't necessarily have to open up the switch to clean the headlight contacts, if you look around it you can see where they are exposed at one side. (Problems with the turn signal contacts would probably require it to be opened.) The switch is actually much simpler than it appears, half of the terminal lugs on it are just dummies that are there to join the cable to the wires that go up the switch stalk for the wiper switches.

I then cleaned the switch contacts and snapped the switch back together. The date code on the switch indicates that it is probably the original unit. Reinstalling the switch was surprisingly difficult, and it wasn't the usual problem of getting the connectors threaded back through the steering column. The knot of the main wiring harness was sufficiently in the way of the big connector that I couldn't get them mated again, I had to remove the female connector from its chassis mount in order to mate them, then I could snap them back into the slot in the bracket. At that point it was easy to put the rest back together. From appearances the turn signal release tab on the steering column is physically centered, so I don't think I need to do anything there. I did plug the warning module back in and I should start putting everything back together, but I was (again) out of time this morning. Tomorrow I won't be able to do anything.

Wednesday, August 20, 2008

I didn't have a lot of time today, but I did get the driver's side kick panel and sill (wiring) cover removed, as well as the driver's carpets and seat, and the center console loosened. With the rear deck removed this exposed the bulk of the old cell phone installation. This all needs to come out! (Jill has requested repeatedly that the dangly wires be removed. Can't say as I disagree with her, it's just been a large bit of Pending Pain. Now that the car was already torn half apart it's Time.)

Thursday, August 21, 2008

I finished removing the cell phone. This required removing the rear bucket side panels in order to un-trap the wires that went back there to where the main unit was. I took apart the handset cradle and removed the connector so I could then push it back through the hole in the center tray. (I didn't want to cut the cable, call it a personal quirk of mine.) The carpet covers up the hole, it looks undamaged. I also removed the antenna, the wire just pulled through into the trunk as it had already been yanked out of its connector.

While I was there I re-routed the speaker wires to go through an open channel rather than be pinched against the chassis by the side panel.

I then had a peek at what it might take to add the rear fog light. The rear taillight assembly is just like the 450 SL's, there's room for an auxiliary brake lamp to be secured behind the parking light bulb. I didn't have any suitable sockets in the junk box, I'll look for one at the store. I still haven't decided whether or not I'll actually do this, but at this point in the car's disassembly it couldn't get any easier.

...Today after work I picked up a single-filament lamp socket that can be adapted to be surface-mount. About $3. (I got one for the 380 SL too, just in case I get ambitious.)

Friday, August 22, 2008

Digging up the information on how I'd done this before out of the predecessor 450 SL's log, I added the necessary two wires to the rear of the headlight switch: NS to go back to a new socket in the left-hand taillight and the 31 (ground) for the indicator lamp in the center of the knob. Reaching the two screw terminals is a real pain, things are just too tight. I used a Sharpie to label all the outer ring of terminals and then removed them. That allowed me to pull back the plastic collar exposing the rear set of terminals. I stole two headlight switch screws from a junkbox donor and crimped some ring terminals on the new wires. It was very tight quarters and difficult to do this job, but I did get the new wires installed. I picked up ground by wrapping a length of stripped wire around the mounting bolt for the steering column. Tacky, but sufficient. When reassembled, the lights worked correctly.

The 'new' wire (actually recycled yellow wire from the cell phone installation I just removed) is threaded down the side of the kick panel and through the wiring channel on the sill, thence up and over the wheel well. It's too short, so I'll splice another length on and run it through the wiring grommet with the radio antenna wire and into the trunk. (I was out of time again.)

Saturday, August 23, 2008

I spliced a length of the cell phone's blue wire to the too-short yellow and threaded it on through to the trunk. I used a wiper blade insert spine (a thin stiff whippy metal strip) to poke around from the antenna grommet in the rear of the well until it came out by the anti-towing sensor, then I taped the wire to it and pulled it through. Just like threading a needle. I fed the wire around the side of the trunk behind the carpeting, it doesn't show at all. Next up was mounting the new socket to the light assembly. Its mounting ears got cut, bent, and drilled such that it mounted flush to the side plate that holds the rear parking lamp, screwed between the existing lamp and its reflector. There's plenty of room. The new lamp globe is directly behind the old one. I put a new pin in the connector in the unused site #8 in the shell, resulting in the neatest possible installation; near-factory in fact except that this particular taillight assembly has heat-staked rivets holding it together so I just broke them off so I could get behind the connector shell. I drilled and replaced these plastic rivets with screws. All the spare male connector pins I could find were a little too fat at the wire end to fit easily into the connector shell, apparently the design style had changed for that connector, but a little gentle persuasion with a hammer made it go anyway. I greased the new bulb's base before I put it in the new socket. The wiring was all soldered, with heat-shrink tubing for insulation. When tested, it all worked properly.

I then started putting the car back together. As I had all morning, and some help, I was able to finish by 2:00 PM. Reassembly went smoothly, except for getting the kick panels in properly; those are tough. Getting the front seat back in and on track was also a bit difficult.

On the road the car behaved well, but the SRS light is on and the engine temperature read low. (It always has.) I'll look into those things next. My plan is to drive the car myself for a few days while I finish the sorting out, then swap with Jill and take the 190D she's been driving down for maintenance. I managed to get the steering wheel back on one notch off.

...While driving at night I noticed that the battery light was on faintly, it may be time for new brushes. But the SRS light was off. The transmission probably needs oil, too, as it shifted oddly at times. And the thermostat definitely needs checking out, the engine temperature was reading low, around 60 °C at times. Things to do!

Monday, August 25, 2008

I went into the garage and found my remaining gallon of Zerex G-05, which I had bought for this car. (No small feat, given the state of the garage.) I also found the new thermostat in the trunk, and the bag of flushing thermostats and the pierced radiator hose (used for flushing). For once I didn't have to do a lot of looking! The rated capacity of the system is 12.5 l, so I don't really have enough G-05 to get a 50% mix. (This March I used up the other gallon I'd bought in the 190D, which has an 8 l capacity and thus did get a proper mix.)

Anyway, I jacked up the car, drained the radiator into a bucket, removed the upper radiator hose, and finally removed the existing thermostat. I could see that it was partially open, hence the low operating temperatures. When I checked my bag of (2) forced-open flushing thermostats I found that this car didn't take either one! So I cut another piece of .38 shell casing and used it to hold the thermostat fully open. I installed this, hooked up the flush hose and a water source, turned on the water and started the car. I put the heater on MAX. I let it run for about a half an hour, until there were no signs of green coming out. (This amount of time was excessive because I'd noticed a green pocket in the reservoir and spent some time removing the low-coolant-level sender to drain that pocket.) I then removed the flushing thermostat and installed the new one, jiggle valve up. (The jiggle valve had been at the 3 o'clock position on the old one, which is wrong.) I used the new O-ring gasket from the thermostat kit. (There was another choice that was clearly wrong.) Before I put back the housing bolts I chased the threads with a die and painted anti-seize on them. The inside of the thermostat housing was free of corrosion, I don't think things had been let go too far. The new flushing thermostat went into the bag with the others.

While I was working on the car I noticed that apparently I neglected to hook the alternator back up to the car. That might explain the dimly-glowing battery light! I put it back and put the battery on charge. (It was thirsty because of the night babysitter run on Saturday.)

As I don't have quite enough G-05 for a complete change and I don't want to risk it anyway until I'm sure there are no leaks, I just refilled the car with water. (Back-filled through the head hose to eliminate head air bubbles.) The drain bucket holds about 6 l, so just draining the radiator and refilling with coolant (once I have some more) ought to get the mixture pretty close. I'll try to pick up some more today.

Since the car was up on jacks I started on the steering wheel centering. I wanted the turn signal cancellation to be centered as Jill had reported that this acted odd, so that's what I used to decide where the wheel went on the shaft. If the wheel isn't centered in use I'll have to adjust the tie rods (equally on both sides) to get the wheel perfectly centered. That might take a few attempts.

While the flush was progressing I checked the transmission fluid level. I'm never any good at this, but I decided that it was low (also corroborated by its shifting behavior) so I added half a quart or so. It's easiest to just pour it down along the partially-removed dipstick as that keeps it from splashing around. I threw the IR thermometer into the trunk just in case I still have engine temperature problems. (I don't expect any, the visibly-bad thermostat is enough to have caused them.) I put in the G-05 too, though I don't expect to do the coolant fill on the road. (It'd be OK, all I'm draining at this point is pure water.)

...I bought two more gallons of G-05 at NAPA, nearly $30 even with the AAA discount! Sheesh. That should give me enough to do both this car and Ethelred the 380 SL. I also bought a Harbor Freight bench brush for removing rain-borne dirt and dust from the soft top. $2, on sale.

The steering wheel is indeed off center, I'll need to adjust the tie rods to bring it back to where it should be.

The temperature gauge now reads normally, something right around 85 °C. The transmission's shifting was also much improved.

Tuesday, August 26, 2008

I jacked up the car, drained the radiator, and refilled with G-05 coolant. I did use a gallon and a half, but I spilled a fair bit. It's 'overfull' right now, but I expect that to burp down. I did back-fill through the head hose to prevent air bubbles. The water that came out still had a faint green tint, this must have been dissolved out of internal deposits as yesterday's flush was pretty thorough.

I then loosened both tie rods and rotated them one full turn each in the direction that would make them steer towards the right. (To match the direction the steering wheel is offset. This meant the car's left side rod needed to get longer, and the right side's shorter. To do this the vise-grip, when clamped to the rod body with the handle facing rearwards and the slack out of the ball joints, has its handle go up and forward over the top, the same action on both sides.) We'll see today if that was the right amount. (I expect it to take a few sessions to get the steering wheel perfectly centered.)

...After work I checked the coolant level, and though it did come down some it's still a bit high. Oh well. If it persists I may let out a little some time, I could put it in another car! (Perhaps Ethelred, it's next up for cooling system service.)

The transmission, though much happier now, still seems a bit anomalous sometimes so I checked the transmission fluid. Near as I could tell it was still off the bottom of the dipstick, so I put in the rest of the quart. Will check it again tomorrow. The tie rod adjustment worked well, I think perhaps another 1/2 turn will do it. After tomorrow's session (and test drive) I expect to be able to turn this back over to Jill, then I can begin to tackle the 190D's most pressing problems.

Driving it, I can again say that this is an awfully nice car. Going back to Ethelred in a day or two is going to be something of a letdown.

Wednesday, August 27, 2008

I adjusted the tie rods another 1/2 turn. (Up and over the top from the rear, making the left rod longer and the right rod shorter, turning the car towards the steering wheel's bias.) We'll see if that does it. It was raining, though, so I didn't drive it to work to see if I'm done.

Got a nice compliment from one of the guys at work on its appearance in the parking lot yesterday. Yes, it is a nice-looking car. (At least, much purtier than Ethelred! The guy did a bit of a double-take as it was the same model in the same spot, but suddenly white and shiny.)

Thursday, August 28, 2008

The weather's improved, so when I got to work today I checked the running battery voltage: 13.8 volts. A little low for modern battery chemistries if you ask me, but within acceptable limits; it may well be the regulator's chosen value. I'll keep an eye on it. I also checked the transmission fluid and it was still low, just covering the curl at the bottom of the dipstick. I put in 1/2 quart.

I overshot on the tie rod adjustment, I think I need to come back about 3/16 of a turn. (It's not as far off to the left as it was to the right, so 1/2 of the last 1/2-turn correction isn't right, so we'll go halfway in between that.)

...After work I got another compliment on the car. Nice.

When I got back home I checked the transmission fluid again and it was still low, about halfway to the optimum level from where it was this morning, so I put the rest of the quart in. I threw a quart into the trunk for emergency on-the-road topping off. That's a good thing on a car with such an apparent appetite for oil.

Friday, August 29, 2008

I rolled back the tie rods 3/16 of a turn and relieved the binding on the driver's seat height adjustment, and told Jill to go ahead and start driving it. I'll miss it!

Sunday, September 14, 2008

Yikes! Jill called me this evening around 5:00 PM, she said she'd run off the road. Turns out it was into the median of the freeway! Somebody had roared up an onramp just where she was changing lanes to the right, and when she caught sight of him "out of nowhere" she overcorrected (so we deduce) and broke the front end loose. She fishtailed for awhile until the front wheel caught the gravel at the median, then it was all over. Witnesses said that she had spun around three times. (That might be 3×180°, not 3×360°, we're not sure. Jill certainly isn't.) She ended up in a cloud of dust at least partially in the oncoming traffic lane on the other side of the median. (There is some question as to which side of the yellow line she was on.) Fortunately nobody hit her and she rolled back down into the median. Shaken, but OK. Several people stopped, one offered her some baby wipes to wash off with. Jill wondered why, then she figured out that she was completely coated in dirt. That witness said she thought Jill had rolled because of the huge amount of dust and how dirty the car was when she stopped to help.

For extra fun some looky-loos got clipped, so there was an additional accident right there with people standing around. It was all gone by the time I got there, I don't know much more about that. (So far as the original incident goes I suspect mutual culpability. Jill was probably inattentive as to where is or is not a good place to change lanes, and our Masked Driver was probably speeding.)

When the Idaho State trooper stopped she noticed a fluid running out of the car back by the exhaust pipe, the deduction (not sure whose) was gasoline and the car shouldn't be driven. That's when Jill called me, and I told her to call AAA. I then went out and hooked up the car trailer to the truck and headed out with Daniel. AAA only covers 5 miles free, I figured maybe we could transfer the car to our trailer in a safe quiet place. I called from the road and Jill was a lot calmer by then. We determined that since the trooper said it was OK for us to just load the car on the trailer ourselves right there in the median that we would try. So Jill called AAA again and cancelled the tow (which was still some 40 minutes away from the North side [idiots, who sends a Northside tow for an Eastside incident anyway?]) shortly before I drove by the two cars in the median, turned around at that next exit, and joined them. (That was hard, crossing the freeway from that same semi-blind onramp without getting hit. I think I got flipped off a few times.)

I've never seen a dirtier car, it was just filled with dust and dirt, like sombody'd tossed a bucketful over it. The wheels all had dry grass stems sticking out from around the rims, wedged in during the spin. I went around the car, there were no signs of damage. I couldn't see or smell any gas. I popped the filler cap and heard a 'whoosh'. I started the car, it ran fine. I went around and crawled under, and couldn't see any gas leak with the car running. There was a drip from the bumper, that's what the trooper had been seeing, but I tested it and it was water. After some head-scratching I couldn't see any reason not to, so we thanked the trooper and Jill drove off in a big cloud of dirt, most of that coming off and out of Jill's car. I followed her to keep an eye on how the car drove. (It was fine.)

There was no ticket, nor a police report since there was no apparent damage. We went to our favorite fuel stop, it was close by and I needed fuel anyway. I figured I'd give it a more careful look there.

I went around again. I couldn't see any damage except a rock hole in one headlight, and that could well have been there from before. I noticed that the drain plug from the spare tire well was wet so I opened the trunk. Wet. The gallon of water that had been riding around back there since the July 14 overheating incident had burst. It was a heavy polyethylene, much thicker than the milk jug that it resembled. Mystery explained! There must have been some significant forces involved in order to pop the jug, though obviously nothing really traumatic. The car is low, wide and heavy, so it just went into a flat spin instead of digging in and flipping as an SUV or mommyvan probably would have done. (Or for that matter our truck, but we only drive that when we need it so our exposure [so to speak] is limited.)

We went on for ice cream which gave Jill some time to clean up and calm down. When we got home she parked in the lawn and we gave the car a thorough cleaning, or as thorough as one can be in the dark. Sucked out the dirt, wiped down the interior with a damp rag, and washed the car. I left the trunk open to dry out, parked outside in the breeze.

By tomorrow it "won't have happened", except that she lost her hat. Too bad, it was a cute cowgirl number she got recently at Goodwill. It was fun to see her roaring along in the convertible in her fancy hat. I'm not sure she'll be able to replace it anytime soon, considering the source.

Monday, September 15, 2008

I looked over the car in the daylight. Much more vacuuming required, and some dust to wipe off inside. (Daniel manned the vacuum last night, he had fun he but isn't the most thorough of workers.) Since the oil was low and it was time I changed the oil and filter, and I did it from below so I could look everything over. (You have to go below anyway if you're going to change the filter.) Everything looked OK, but I think there's a loose ball joint on the center drag link, so I put that on the list. I did dig a bunch of fresh dirt out of where it was jammed into the air dam. I topped off the washer fluid, it was low. I'll be driving the car today to check it out on the road.

...It was fine. We traded cars at lunch. I do believe she prefers hers to Ethelred!

Tuesday, September 16, 2008

The driver's side windshield washer nozzle heater assembly had its neck broken off, hence the no squirting on that side. I pulled off the two broken pieces, dried them, and Shoe-Goo'd them back together. I set it aside to dry. I then put the trunk back together as it's now all dry.

Wednesday, September 17, 2008

I reinstalled the squirter's heater. It should be fine now, it squirts at least. I replaced the now-dry trunk's contents, and replaced the batteries in the flashlight (which somehow got left on).

Sunday, September 21, 2008

Sadly, the rains have finally come putting an end to our magnificent run of early fall weather, so it's time to put the lid back on the car again. C'est la vie.

I got out the touch-up paint and fixed a couple of small chips in the paint that I found while dusting off the car.

Monday, October 6, 2008

The brake fluid was again low so I refilled it. Odd, there's no overt signs of leakage.

Wednesday, October 8, 2008

Jill's been reporting a disturbing rattle up front, so I jacked up the car and had a good look around. I didn't find anything other than the barely-loose drag link. (I used a rubber mallet to bang on this and that.) I did wonder if the heat shield around the crossover exhaust pipe was loose enough to rattle, so I wedged a few pieces of sheet metal into the gap on the end and put a hose clamp around it to secure it all. We'll see. I also topped off the low power steering fluid, it had been groaning a bit lately.

...No, driving it today I could still hear the rattle. Sounds more like loose bits inside the dash. Heavy bits.

Sunday, October 12, 2008

Jill was reporting that the low-oil lamp had been flashing so I checked. The oil was low, I put in a quart or so. It has only been about 1200 miles since the oil was changed, I guess it's either leaking or burning it.

Thursday, October 16, 2008

I ordered a new steering drag link from Rusty. $75.

Monday, October 20, 2008

We recently bought a new washing machine, replacing the 1974 Kenmore. My wife's been complaining about the box in the driveway, which I'd been saving for new drip pads for under the cars. Today she got one!

Tuesday, October 21, 2008

I opened the box that came yesterday, and found the drag link. OK, I need to find some time to do this now. Saturday?

Saturday, November 1, 2008

Flash-to-pass isn't working. Fuse?

Tuesday, November 4, 2008

Oil and brake fluids were low, topped them up again. It's got an appetite! Nothing visibly wrong with Fuse #2, the one that runs the flash-to-pass switch. The same one runs the wipers and washer, so it's probably OK. Switch problem? This is the switch I operated on, after all...

Monday, November 10, 2008

So, today I decided to do something about the rock pip I'd found in the left high-beam headlight after Jill's off-road adventure. New headlight? Well, you'd think so, but that's just not my way. There was water inside the glass so I pointed a heater at it and taped a straw to the air compressor to heat the lens and run air into it to evaporate the water. I then removed the lamp and shook it to get all the tiny glass chips out the little hole in the front, except for the two big chips that couldn't come through such a small hole. I then rattled them around until I got the big chip back into its crater, then I squirted Shoe Goo in to seal the hole and glue the chip more-or-less back into place. I placed the headlamp face-down to let the glue set up. The other chip can just rattle around loose in there. We'll see how it goes.

I hate waste, even to the point of repairing a stupid cheap USDOT headlamp!

Tuesday, November 11, 2008

The hole wasn't completely sealed, so I put a little more Goo on it and pressed it in. After it set up a bit I put the lamp back on the car.

Monday, June 1, 2009

Jill's been bugging me to get this car out of storage, so today I finally managed it. (I moved crap out of the way yesterday and put the battery on charge.) It started immediately, with no fuss. It was very dirty, so I ran it into what's left of our front yard and washed it there. There were a few dings on the door edges, so I got out the touch-up paint and covered them.

Friday, June 12, 2009

Took the top off for her. (I've been lax.) Maybe now she'll drive it.

Wednesday, July 29, 2009

I went out to get the battery charger (for the boat), and found the passenger car door open and the courtesy lights (naturally) burning. How long's it been that way killing the battery? At least since yesterday morning. I put the charger on the car instead, it definitely needed it more than the boat.

Friday, September 18, 2009

It's been nearly forever, but after moving into the computer room I found the sketch for the user-selectible always-on modifications to the rear window defogger relay that I worked up May 26, 2007 that would be useful in powering a travel cooler on road trips. (See also the 190D's Road Trip Relay for another take on this problem.) I used a 28-280 Radio Shack breadboard system that I bought at the thrift shop ($9) for this purpose (and perhaps for eventual gift to my son), and components salvaged from the junk box. Unfortunately, it didn't work right. Par for the course when it comes to my designing old-fashioned transistor circuitry. Needs more work, obviously...

Saturday, September 19, 2009

With fresh eyes I can see that I left a bias resistor out of the circuit. With that in place it started working correctly. I tinkered with the component values a bit and got it working reliably. When the STOP signal is asserted for a little more than one second it turns on, it turns off immediately when the STOP signal is asserted momentarily. The circuit powers up in the off state reliably. The schematic of the final (!) relay, for future reference, is in Illustrator, PostScript, PDF, and GIF formats. Now I just need to make one!

The Theory of Operation for the new circuit is that while the STOP signal is asserted the new capacitor C3 charges up slowly to a threshold set by Q3 and the 6 V Zener diode D7. When Q3 fires it trips (through R10) the latch formed by Q4 and Q5, which supplies power to the original timer relay circuit, engaging it (via D8) and feeding voltage into its timing capacitor (via D9) to prevent its normal timeout. C3 then discharges through Q3's base-collector junction and Q5, ensuring that Q3 won't be hovering near activation and perhaps interfering with attempts to disengage the latch. While STOP is unasserted C4 develops a considerable differential voltage across it through the agencies of Q4, R1, and R2. Whenever STOP is first asserted this voltage pumps the base of Q4 sufficiently positive to ensure the Q4/Q5 latch disengages, and so long as STOP is released before Q3 fires the disengagement will hold. The circuit exhibits the desired behavior, a toggle ON-OFF action, with a delay before ON. However, there are a couple of lingering concerns:

  1. Can Q4 supply enough current through D9 to actually trip the original defogger timer? There is the relay coil itself to power, and also the lamp in the dashboard switch.

    This can be addressed by beefing up Q4, perhaps in a Darlington configuration with a bigger PNP transistor (as Q6).

  2. While STOP is asserted can the original timer circuit engage at all?

    This might require another diode (D10) from the collector of Q5 to the base of Q1, which will hold it ON while the latch is engaged, thus allowing the relay to be powered. When the latch is released (via C4), Q1 should be able to process the normal STOP signal that it will then be seeing.

  3. Will C4's initial discharged state cause the latch to trip upon power-on as it attempts to charge itself through R1 and R2, and pulls current through Q4?

    I sure hope not! This can be tested with the prototype circuit merely by putting a 4700 ohm resistor between the STOP signal and ground.

These questions will be answered once I actually build a modified relay.

Tuesday, September 22, 2009

I got out the prototype board again, which had been off for several days, and when I flipped on the power the circuit came up engaged, which is definitely undesireable behavior! After that it behaved normally. I put the 4700 ohm R1/R2 test resistor into the circuit, and with it in place things did not look good! The circuit would often power-up with the latch engaged, and it wouldn't stay disengaged once the STOP signal was released. A setback! This is probably all due to unintended action of C4, as the circuit resumes normal ON behavior if it is removed.

I added a diode (D10) to prevent C4 from drawing charging current through Q4, and gave it its own weak charging resistor (R13) instead. That restored normal toggling behavior, even with the R1/R2 analog in place.

Wednesday, September 23, 2009

When I flipped on the power the first time today the circuit came up engaged again. This can't stand! Speculating that parasitic or leakage effects are somehow 'encouraging' the Q4/Q5 circuit to latch as power rises I added C5, a small capacitor across the base-emitter junction of Q4, which should tend to hold it off. (C3 is definitely holding Q3 off as power comes up.) It's small enough, however, that it's easily overridden by strong deliberate action taken by Q3 or C4. The circuit behaved properly after this addition, time will prove whether or not this makes power-on more reliable.

Thursday, September 24, 2009

When I flipped on the power today the circuit came up disengaged, as intended. So far, so good!

Wednesday, September 30, 2009

I've been testing the circuit daily, and it's worked every time. I think I'll call it good for now.

It's cold now, I put the hardtop back on the car.

Tuesday, January 5, 2010

More brake fluid. Also needed a quart of engine oil and a bunch of windshield washer fluid.

Friday, April 2, 2010

I was fetching the cupholder for the road trip in Ethelred, and noticed that the courtesy lights were dim orange. Oops, I haven't been keeping an eye on the battery, and the tender is not hooked up. I put it on charge, it was drawing 10 A, the maximum for the charger.

Wednesday, April 21, 2010

Jill said that she wanted to switch to this car for the season, so I took the battery charger off, pumped up the tires, and checked the fluids. I blew the dust off with air, no sense washing it since it looks a bit like rain today. Will leave the hardtop on for the same reason.

Wednesday, April 28, 2010

Beep-beep-beep-beep...

Jill says that the car's factory-supplied alarm has been going off at times. (It's probably not being properly disabled by the door's key switch, said door switch is likely dirty.) Today I had a chance to look into it. These things are widely considered useless, and annoying, the usual (and least expensive/troublesome) solution is to disable the alarm entirely by unplugging the alarm's brain. According to the ETM (second half, page 128) it (N26) has two connectors, an 8-pin and a 14-pin. The schematic shows nothing that looks like it's in series with anything important, so unplugging it (both connectors) looks like the right thing to do. The component location guide's page 202 shows it located behind the glove box. The photograph (page 218-1) shows it to the upper left of the junk back there, somewhat towards the front and with its plugs facing forward.

Glovebox? I can do that. A few minutes later I had the plastic buttons popped out (with my trusty antique carbon-steel butter knife) and the liner out. Detailed examination showed the black plastic Becker Autoradio unit to be screwed to the top of the plastic air duct, connectors forward. I unplugged it.

For extra credit I removed it to have a more detailed look. Two stickers, one bearing:

(M)MERCEDES-BENZ
126 820 08 26
72BAW 845 Z 0000
GEPRÜFT: 2086

and the other bearing:

BECKER
AUTORADIO
BrandEDW-Steuergerät
Typ
Model-No.
0845 509.485
Geräte-Nr.
Serial-No.
T 20132306

After releasing the two plastic snap-hooks I could slide the board out of the shell, and I found about what I expected. Many 4000-series CMOS IC's: Two 4013's, two 40106's, two 4001's, and one each 4060, 4069, 4002, and 4012. Also about 35 signal diodes, 6 zener diodes, three rectifier diodes, two transistors, four relays, one large (troublesome) Frako electrolytic capacitor, two smaller electrolytics, and the usual handful of resistors and capacitors. All jellybean logic, in other words. Should be very easy to repair, if one were ever inclined to do so. (And I suspect that this car's problem is in the key switch, not the alarm brain.)

QtyTypeDescription
(2)4001Quad 2-input NOR gate
(1)4002Dual 4-input NOR gate
(1)4012Dual 4-input NAND gate
(2)4013Dual D-type flip-flop
(1)406014-bit ripple counter, with RC oscillator
(1)4069Hex inverter
(2)40106Hex Schmitt trigger inverter

4000-series CMOS logic is ideal for this purpose because it has very low quiescent current draw, and can run directly off of the car's battery voltage so there's also no power-wasting voltage regulator. As a rough guess, the various Sense and Arm/Disarm inputs from the car go through the Schmitt inverting buffers and are massaged by the gates down to three signals Arm, Disarm, and Trigger. The flip-flops probably keep the Armed/Disarmed and Triggered states. The ripple counter generates the honking/flashing pattern when Triggered, and drives the relays through inverting buffers and the transistors. (The relays drive the horn and lights.) The ripple counter is also probably responsible for the Triggered timeout, so that it won't run forever once Triggered. My guess is that the RC oscillator is disabled except when the circuit is Triggered, and so there is no power consumed but for the circuit's DC static requirements while Disarmed, or Armed and un-Triggered.

I snapped it back together and put it back in the car. (Unplugged, of course.) I buttoned the car back up and called it good. (I bolstered the positive terminal insulation of the glove box light with heat-shrink tubing. It was, as is so often the case, coming loose.)

Wednesday, May 5, 2010

Jill complained that the driver's seat felt loose. I looked, and found that the right front pivot bolt had worked loose. I tightened it, that should be better.

Thursday, May 13, 2010

Finally it's time to take the lid off this car. The nylon straps of the lift are shrinking a bit, and it gets harder and harder to get them onto the top. The secret is to put the two side hooks on first, well back of their normal position, then slide them forwards until you can engage the forward hook.

Sunday, May 16, 2010

It was past due, and I finally changed the oil, but didn't change the filter. I used the vacuum sucker, it took quite awhile because I was only able to warm the engine for a few minutes before I began.

Jill also had noted that the AC didn't work so I checked, and the charge had leaked away. I replenished it, and using a watering can against the condenser and having Daniel keep the RPM's at 2000 I was able to get it down to 37 °F, which is plenty good enough. Ambient temperature was about 80 °F

I topped off the windshield washer fluid with water and checked the brake fluid level, which was OK.

Friday, June 25, 2010

Jill and Daniel took the car to Wyoming for a mini-vacation, and on her way back she called me from Missoula, three hours away from home. The car wouldn't start, and the aftermarket alarm (an inseparable part of the keyless system I'd installed) was honking away at her. I ran her through the basic diagnosis procedure with the lights, neutral switch, etc., but didn't get good results. (A lack of calmness doesn't help.) Then I had her get out the cheap Harbor Freight multimeter I keep in the trunk, and the battery measured around 10 V. Oops! She called AAA to get a jump, and the guy knew what to do. He checked the battery voltage once it was running and it was 13 V or so, enough to prove that the alternator wasn't totally dead. She got home (carefully husbanding the battery charge) without further incident, and I put the car on charge. It was thirsty, but not inordinately so. It probably needs a new brush pack, they usually get intermittent at their end-of-life.

While I have already disconnected the factory car alarm, the aftermarket keyless entry system also has a built-in alarm function, and that was going apeshit when the battery was low. I only have the alarm horn connected because it's required in order to be able to train the key fob, and it normally doesn't beep the way I have it programmed, nor are the alarm sensing wires even connected. But when it went nuts it sure made noise! Repeatedly.

I got out the soldering iron, and a slide switch I'd gotten at a yard sale. (In a baggie with several other switches, all for $1.) I cleaned the switch with brake cleaner and put it in the alarm's horn wire, that should cure that little problem. I labeled it with a Sharpie, and made sure it was in the OFF position.

The battery box lid was all broken up, and filthy, so I pulled it out and washed it, and started gluing it back together with Shoe Goo. I note that the battery is sitting on a piece of plywood inside the box, that makes it protrude a bit more than normal, and which might be responsible for why the battery cover got so badly broken. I'll have a look at that, when it's time to put the cover back on. I think only a couple of small coin-sized pieces of the cover are missing, the rest seems to be there.

Saturday, June 26, 2010

I dedicated the day to gluing up the battery box lid. There were a lot of cracks! I got the bulk of it glued in a number of sessions and then clamped it to a flat board to let the glue set hard overnight in position. That'll get it flat again, it was considerably warped. Still a lot of gluing to do, though. I'll probably end up exhausting my tube of Shoe Goo on it.

Sunday, June 27, 2010

The overnight set-up seems to have worked, the lid is fairly straight now. More glue and clamps today...

I pulled the battery and battery box out, which required removing the ground cable from the chassis. The NAPA 75 Group 49 battery has a June "2" date code, probably 2002. The box itself is cracked in a few places, which I'll want to repair. The battery was sitting on a perfectly-fitting board of some kind of dense red plastic, not plywood, perhaps this is factory original? More research is required. I found one of the two missing chunks of the battery box cover, and a tiny piece of the other one, the rest of it seems to be gone. The area is very dirty, and a good vacuuming is in order.

I washed and dried the battery box, and began gluing it too. It won't need much repair, unlike its lid.

Monday, June 28, 2010

More battery box and lid gluing. Takes a lot of sessions to do it 'right' when it is as tattered and deformed as this one was. I have to clamp the lid to the board, sometimes with spacers, to get it to dry back in shape, and I have to leave it for quite a while in order for the glue to have top strength before removing the clamps. All that's left to do now is one strip on the side lip of the box lid, and maybe some spot bolstering, but I'm pretty much out of glue. I'll get more today. I also bias-cut and glued (with cyanoacrylate glue) the box's broken EPDM sealing ring.

I then moved out to the car, and removed the alternator. To do so it's easiest to first shift the windshield washer tank out of the way, then it's just one 13mm and two 17mm bolts and unplug it. With it out of the car I could then get at the two screws that hold in the combination regulator/brush pack, and with that out it was obvious that it was worn out: one brush was much shorter than the other, and its corresponding slip ring was a bit chewed from arcing. I'll need a new brush pack, and to dress that ring. It's a 70 A unit. (Marked 14V 28/70A, I wonder what the "28" is?")

...I checked at Schuck's, and they now want $61, plus a week and $6 shipping, for a brush pack. A front bearing is now $30, same deal. No thanks! Rusty's price for the brush pack is more like half that. I checked at Ace hardware for individual brushes, and it appears that they've stopped carrying those. Jerks. I need to assess the state of the bearings before I can decide my best course of action.

I bought more Shoe Goo at Ace, while I was there. ($5) When I got home I glued on the last piece of the lid. Later, after it had set up, I started bolstering the weak points. I also pulled off some glue that had started to come loose due to overexuberant clamping, and perhaps a bit of poor surface preparation. I'll finish by putting that back.

Tuesday, June 29, 2010

I re-glued the bad spots on the lid. I then just had to deal with the missing chunk. I found a piece of scrap black plastic (the tray face from a dead DVD player!) and cut some chunks that filled the hole, then glued them in place. That pretty much finished up that job.

When spinning the alternator by hand it sounds 'dry', I'd say that it really could use a new bearing or two. Checking my records I find I've done this before, three years ago on the 190D, and the place to take the alternator is Spokane Auto Electric & Repair (1407 E. Sprague). They carry everything, and can turn slip rings too. I just need to take it apart and re-assemble it.

Not an issue. Step one: use a Sharpie to mark the phasing of the two housings. As before, I then put two screwdrivers into the fan and set them against bolts through the alternator mounting holes. A 22mm box-end wrench went over the nut, and then a hammer striking the wrench removed the nut easily. (Inertia, not so much force on the fan, was the counterforce.) The pulley, fan, and all the spacers just drop off the front then. I strung them on a piece of wire to keep them in order. A hammer and a screwdriver removed the shaft key. Removal of the fan exposed the four screws that held the body together, those came out easily enough. (Don't slip and bugger the screw slots, or you'll really have a problem!) A brass hammer tapped around the rear housing caused it to drop away from the front housing and rotor, the rear bearing stayed with the rotor. The rear bearing was very dry, it's close to failure. Most of the grease appears to have worked out of both bearings. I removed the four little screws that released the front bearing clamping plate, and with the nut on the shaft the brass hammer drove the front bearing out of the front housing.

Checking the tool box I found a recently-acquired New Britain puller (50¢ at a garage sale) that is a perfect fit to the rear bearing. It clipped over it and with a twist and a little pop it came right off the shaft, the flat end of the puller's bolt slipped perfectly through the bearing. (It was sweet, I love using good tools!) The front bearing is the hard one, but I have found that I can use a clamp-together flat plate bearing puller in conjunction with a 2-jaw puller to pull them off their shafts. I kept the front nut half-on the shaft in order to constrain the point of the 2-jaw puller. It took quite a bit of force, but the bearing pulled off pretty easily, and the procedure didn't seem to deform the bearing clamping plate too much. Disassembly complete; it didn't even take very long.

I put the rotor, bearings, and brush pack into a box in the trunk of the car.

...Today out at lunch I stopped by Brown Bearing, and unlike last time they had both alternator bearings. $15 for the pair. I stopped by Spokane Auto Electric & Repair, and they did not have any solder-in brushes, but they did have the brush pack for $30, which is an OK (but not great) price as these things go. (They did say that it was made in the USA. Marked 71-40007 and USI 00838.) I bought it so that I can finish (?) tomorrow. They didn't think the slip rings needed turning, but they did recommend that I chuck it in a lathe and use emery paper to take off the black. I think I may be able to rig something, we'll see.

Wednesday, June 30, 2010

I slipped the old front bearing back on part way, wrapped a strip of pop can metal around the back shaft, and chucked the rotor into the drill press as a vertical lathe, with the front bearing resting on the table and the shaft protruding through its central hole. I then got out a flat stick and some emery paper and had at it. That worked, but it exposed the fact that the one worn slip ring had a noticeable crease in it, presumably from arcing. I got more aggressive with a file and flattened it, mostly, then re-applied the paper and stick. (Taking the hairline groove completely out would have removed more material than I was comfortable with doing.) I now have a nice shiny smooth, and mostly flat, pair of slip rings. We'll see later if I made a mistake or not! I didn't have time to do much more.

The original front bearing was marked FAG 6303.R.10.18, and also A.Q and ITALY; one dust cover is marked 6303 S 457, the other 6303 S 478. The replacement is also FAG, labeled on the box 6303.2RSR.C3 but marked on itself 6303.C3 and E275-0331 HB; one dust cover has 6303RSR and W263 on it, the other has 6303RSR and W243 on it.

The original rear bearing was marked SKF 6201-2RS1/C3HT228VU035 (a bit sketchily, as it's on the outside of the race and has some scuffing that somewhat obscures the legend), and also B (or 8) and ITALY, the dust covers appear to be unmarked. The replacement is Koyo, labeled on the box 62012RDC3 but marked on itself only C3; the dust covers have 6201RD, KOYO, and JAPAN on them, once side also has 555 and the other has 519.

Thursday, July 1, 2010

Reassembly time! I cleaned the shafts of the rotor and put it in the freezer, and put the bearings and housings in the shop oven at 200 °F. They just slid together after that, with only a little tapping with a hammer and some deep sockets to seat the bearings fully in place on the rotor. You definitely want to make sure to remember to put the captive retention plate on the front shaft before you put on the bearing! The body reassembled easily then, the worst part was getting the little half-round key into the shaft's notch. It is interesting that the belt pulley is two separate sheaves, I didn't notice that before. The alternator spins smoothly and quietly now, it's nice. I then put it back in the car, nothing special about that procedure.

I checked the fit of the battery in the box, and I found that with the red plastic spacer board in place the lid didn't even come close to fitting down over the sealing lip of the box, which explains how it had gotten so broken up: they'd tried to buckle down the lid but it wouldn't go, and they tried forcing it. I imagine that what had happened is that at some point someone had put in an incorrect battery, a small cheap one rather than the correct (and rather large) Group 49, and that the cables didn't reach the posts so they'd put the board in to lift the battery up a bit to reach the cables. Later, when the correct battery was installed the board was not removed, and thus began the destruction. With that all figured out I then wiped the battery compartment clean with a damp rag and reinstalled the newly-repaired battery box, then the battery. As I've found before, the hardest part was getting the positive grommet back in the box. I touched up the paint on the buckles, etc., and reinstalled the hatch cover and the buckles. I brushed off the end of the negative cable and put it back, using some anti-sieze on the bolt.

To maintain the clocks, etc. the car's been on the battery charger this whole time, but set at 6 V to keep the voltage peaks down since the battery wasn't there to serve as a filter. Seems to have worked, anyhow.

I was going to put the used front bearing into the junk alternator that's been underfoot for quite some time now, only to find that it's not the front bearing that's loose! The bearing socket in the front housing is what is loose, the bearing probably got tight and spun in the housing at some time and chewed it out. It's possible that some shimming would restore it, but it's not like I really need it at this point.

I then fired up the car and checked the running voltage, it was 14.3 V which is right in the pocket. Done! I tested the keyless entry fob and it was working fine, once I tried it a few times. (The keyless system sits loose in the battery compartment, all the messing around back there doesn't seem to have hurt it any.)

Thursday, July 8, 2010

It seemed to me that the starter barely turned the car over when Jill drove off from meeting me today. I checked and the alternator light is working correctly, I need to do more checking.

Friday, July 9, 2010

I measured the battery voltage, it was 13.1 V which should be OK. I put the battery charger on, and while it did draw a charge it dropped off fairly quickly. Nothing seems wrong there. I did put a quart of oil in the engine, it was low.

...Jill called me at lunch from the library parking lot, and said that the battery (that went through Hell with the alternator incident) made a big 'pop' noise when she went to start the car, and fluid started dripping out of the back. (It also wouldn't start, and had been getting difficult to start recently, and could sometimes barely turn over though the voltage and charge state always seemed OK.) Sheesh! I got there and opened it up, and the newly-repaired battery box had contained all the acid from the 8-year-old NAPA battery's case blowing open! It had cracks and fractures all over the place, and had leaked thoroughly. We got a pan of water and sluiced it off before lifting it out onto the ground, and diluted the acid stream that was running away from the car. I put the battery on one of the rubber winter floor mats in the trunk of my car, and we went off to Les Schwab where we bought another Group 49 battery for $108. (I washed off the floor mat with their hose.) It installed easily enough into the car, but the cables didn't reach well and I didn't have time to fuss with it. (It's possible that the new battery is a bit shorter than the old one.) It got her home, anyway, but the car wouldn't start again there because the positive cable had popped off sometime along the way. The battery box and the lid have some new cracks in them, so I'll have to do some more gluing too. Before she drove off with the new battery I checked the charging voltage, and it was steady at just over 14 V, which is good. This implies that it was not the rebuilt alternator that killed the battery.

Exploding battery, that's another first for me.

The current theory is that one of the internal bus bars broke a while ago, isolating a substantial part of one cell. That would have put extra stress on what was left in circuit: both heavy starting discharge and the later recharging current would have been forced into a too-small area, eventually causing hydrogen-oxygen dissociation. The working part of the broken cell could possibly even have been driven into reverse polarity during starting by the power of the remaining five cells, and they really hate that. The starting current ability of the battery would have been severely compromised (as it appeared to be) yet the resting terminal voltage would have been fine (as it was). She hit the starter, the diminished cell's voltage dropped precipitously, and minute vibration and/or thermal effects induced the bad connection to re-connect at that moment in an explosive atmosphere of the freed hydrogen and oxygen, and the isolated parts of the cell were (let's say) fully charged and so there was plenty of voltage difference and thus current flow and thus a spark... Check, check, and check! Works for me.

The jouncing the car took during Jill's off-road adventure was probably ultimately responsible for this, though it was only yesterday that I noticed anything odd about the battery. That battery had had a hard life, what with the parasitic drain issues, the eventual alternator strike, and the bouncing around.

Saturday, July 10, 2010

I removed and cleaned the battery box, and began gluing again. It won't take long this time.

...In the afternoon I finished the gluing.

Monday, July 12, 2010

I got a chance to reinstall the battery this morning. I checked the height of the battery in the box, and it's a bit too short thus explaining the problem with the battery cable fit. I put the offending red spacer board back in, and it helped a lot. The battery cables went on easily this time. I buttoned it all back up and vacuumed out the trunk. The battery hatch knob had broken off during this incident, it's rather chewed looking where it goes into the latch hook, but I think it's still usable. I reinstalled it, anyway.

Tuesday, July 27, 2010

Brake fluid was low, I topped it off again.

Wednesday, September 8, 2010

Getting cold out. Put the hard top back on, and added two quarts of oil to the engine.

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